Cessna 402 Safety Record
Complete NTSB accident and incident history. 325 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 12, 2002 | Albuquerque, NM | N38CJ | Incident | substantial | The failure of the left main landing gear scissors assembly which resulted from improper maintenance. |
| Jan 23, 2002 | Bronson, MI | N371JD | Fatal (1) | destroyed |
The maneuver to avoid the utility wire while maneuvering resulting in an inadvertent stall and subsequent impact with the ground. Factors were the pi…The maneuver to avoid the utility wire while maneuvering resulting in an inadvertent stall and subsequent impact with the ground. Factors were the pilot's inadvertent activation of the elevator trim, resulting in a loss of control during flight in instrument meteorological conditions, as a result of pilot's lack of knowledge concerning the operation of the autopilot system. Another factor was the utility wire. |
| Nov 15, 2001 | Pasco, WA | N910WT | Incident | substantial |
the pilot's failure to keep the aircraft from touching down short of the displaced threshold, and his failure to maintain directional control after th…the pilot's failure to keep the aircraft from touching down short of the displaced threshold, and his failure to maintain directional control after the aircraft's left main gear tire deflated as a result of impacting the lip at the beginning of the subject threshold. Factors include the deflation of the main gear tire, and soft terrain near the side of the runway. |
| Aug 25, 2001 | Marsh Harbour, BF | N8097W | Fatal (9) | — | Investigation pending |
| Jul 08, 2001 | Boston, MA | N760EA | Minor | destroyed | The pilot's improper decision to waive the wake turbulence hold time, and his subsequent loss of control when wake vortex turbulence was encountered. |
| May 21, 2001 | Walker Cay, BF | N3269Q | Incident | substantial | Investigation pending |
| Apr 26, 2001 | Del Rio, TX | N80Q | Fatal (1) | destroyed |
the loss of control due to a jammed trim tab, which resulted from the failure of maintenance personnel to properly secure the trim tab actuator rod wh…the loss of control due to a jammed trim tab, which resulted from the failure of maintenance personnel to properly secure the trim tab actuator rod when installing a replacement elevator. |
| Mar 03, 2001 | Fort Lauderdale, FL | N108GP | Incident | minor |
Incomplete compliance with a non-mandatory Cessna Service Information Letter by an unknown person resulting in pulling through of the attach bolt of t…Incomplete compliance with a non-mandatory Cessna Service Information Letter by an unknown person resulting in pulling through of the attach bolt of the upper and lower link assemblies and subsequent rotation of the right wheel assembly. Additionally, improper overhaul of the right main landing gear actuator by an unknown person resulting in collapse of the right main landing gear. Findings in the investigation were: 1) Inadequate compliance with a Cessna Service Bulletin (SB) by company maintenance personnel for failure to replace the actuator as addressed in the SB due to a discrepancy with the actuator noted during the post incident testing, and 2) Failure of the FAA to include inspection of the main landing gear torque links in the FAA approved inspection program as described in the Cessna Progressive Care Program. |
| Feb 20, 2001 | BILLINGS, MT | N69316 | Incident | substantial | Best rate-of-climb single-engine speed was not maintained. Delayed remedial action was a factor. |
| Jan 30, 2001 | Edgartown, MA | N6837Y | Serious (2) | destroyed |
The pilot's failure to maintain a stabilized approach with an adequate vertical and lateral track. Also causal was his failure to maintain obstacle c…The pilot's failure to maintain a stabilized approach with an adequate vertical and lateral track. Also causal was his failure to maintain obstacle clearance. |
| Jan 09, 2001 | Ontario, OR | N6384X | Incident | substantial | Pilot's failure to maintain aircraft control while landing. Factors include a snow covered runway. |
| Dec 20, 2000 | NOSARA, CS | N908AB | Serious (2) | destroyed | Investigation pending |
| Jul 08, 2000 | VIEQUES, PR | N405MN | Fatal (1) | destroyed | The airplanes entry into an uncontrolled descent for undetermined reasons from which it crashed into the ocean. |
| Jul 08, 2000 | DEL CITY, TX | N402NA | Incident | substantial |
the total loss of engine power on both engines during cruise due to fuel starvation as a result of the pilot's improper use of the fuel selectors. Co…the total loss of engine power on both engines during cruise due to fuel starvation as a result of the pilot's improper use of the fuel selectors. Contributing factors were the pilot's lack of familiarity with the aircraft, and the lack of suitable terrain for the forced landing. |
| Jun 30, 2000 | NAPLES, FL | N7037E | Incident | substantial | an inflight collision with a bird during descent that resulted in substantial damage to the airplane's vertical stabilizer spar. |
| May 22, 2000 | CORDOVA, AK | N402ET | Incident | substantial | An in-flight collision with a bird. |
| Mar 23, 2000 | SAN JOSE, CS | N908AB | Incident | substantial | Investigation pending |
| Mar 16, 2000 | SAN ANTONIO, TX | N11NX | Incident | substantial |
The pilot's inadequate handling of the aircraft during the landing flare/touchdown resulting in a hard landing that collapsed the left main landing ge…The pilot's inadequate handling of the aircraft during the landing flare/touchdown resulting in a hard landing that collapsed the left main landing gear. |
| Mar 16, 2000 | FORT LAUDERDALE, FL | N251RS | Minor | substantial |
Separation of the right main landing gear tire recap during takeoff resulting in the pilot's loss of directional control, the aircraft departing the r…Separation of the right main landing gear tire recap during takeoff resulting in the pilot's loss of directional control, the aircraft departing the runway, collapse of the landing gear, and collision with the airport fence. |
| Sep 25, 1999 | CHICAGO, IL | N6362X | Incident | minor | THE FAILURE OF THE PILOT IN COMMAND TO MAINTAIN CLEARANCE WITH GROUND OBSTRUCTIONS. |
| Jun 23, 1999 | VAN NUYS, CA | N186BA | Minor | substantial |
The pilot's inadequate fuel management that resulted in fuel exhaustion and the subsequent collision with vehicles during a forced landing on a city s…The pilot's inadequate fuel management that resulted in fuel exhaustion and the subsequent collision with vehicles during a forced landing on a city street. |
| Jun 08, 1999 | FORT LAUDERDALE, FL | N440AB | Incident | substantial |
The pilot's decision takeoff with condensation on the cockpit windows which restricted visibility, his improper use of aileron control, improper compe…The pilot's decision takeoff with condensation on the cockpit windows which restricted visibility, his improper use of aileron control, improper compensation for winds during takeoff, and his failure to maintain directional control during takeoff, resulting in the aircraft running off the left side of the runway, colliding with a taxiway sign and ditch, and collapsing the landing gear. |
| Apr 27, 1999 | GOLDSBY, OK | N819BW | Fatal (1) | destroyed |
The fatigue failure of the right wing spar as a result of inadequate quality control during manufacture of the spar. A factor was the inadequate insp…The fatigue failure of the right wing spar as a result of inadequate quality control during manufacture of the spar. A factor was the inadequate inspection of the right wing by maintenance personnel, which failed to detect the crack. |
| Apr 20, 1999 | FORT LAUDERDALE, FL | N744MA | Minor | substantial | A loss of engine power due to fuel exhaustion and the pilot in command's failure to ensure that the aircraft had adequate fuel to complete the flight. |
| Dec 23, 1998 | SAN JUAN, PR | N8203Q | Incident | substantial | The failure of the pilot to maintain directional control of the aircraft. The reason for the reported engine surging is undetermined. |