Cessna 177RG Safety Record

Complete NTSB accident and incident history. 244 events recorded from 1982 to 2025.

244

All Events

129

Incidents

38

Minor

25

Serious

51

Fatal (100 fatalities)

Date Location Reg# Severity Damage Probable Cause
Apr 02, 2022 Gaithersburg, MD N123LS Minor substantial
The pilot’s failure to maintain adequate airspeed while maneuvering on final approach which resulted in a high sink rate and subsequent collision with…

The pilot’s failure to maintain adequate airspeed while maneuvering on final approach which resulted in a high sink rate and subsequent collision with a fence.

Jul 27, 2019 Fall City, WA N1828Q Minor substantial The failure of the No. 3 cylinder intake valve that resulted in a partial loss of engine power and a forced landing on uneven terrain.
Mar 09, 2019 Land O' Lakes, WI N52047 Minor substantial The pilot's improper fuel planning, which resulted in fuel exhaustion and the subsequent total loss of engine power.
Jul 07, 2017 Vacaville, CA N7532V Minor substantial
The total loss of engine power during initial climb for reasons that could not be determined because postaccident examination of the engine revealed n…

The total loss of engine power during initial climb for reasons that could not be determined because postaccident examination of the engine revealed no mechanical failure or malfunction that would have precluded normal operation.

Aug 05, 2014 Manistee, MI N468LE Minor substantial
The pilot receiving instruction's inability to respond to or compensate for the sudden change in wind direction and speed that the airplane encountere…

The pilot receiving instruction's inability to respond to or compensate for the sudden change in wind direction and speed that the airplane encountered shortly after liftoff, which resulted in a tailwind condition, a corresponding decrease in airspeed, and a reduced climb gradient.

Jul 31, 2009 Black River Falls, WI N2108Q Minor substantial The loss of engine power during cruise due to the number two cylinder piston connecting rod failure for undetermined reasons.
Apr 04, 2009 Ocean Isle Beach, NC N1838Q Minor substantial
The pilot's failure to divert to an alternate airport resulting in the total loss of engine power due to fuel exhaustion. Contributing to the accident…

The pilot's failure to divert to an alternate airport resulting in the total loss of engine power due to fuel exhaustion. Contributing to the accident were the pilot's incorrect determination of the fuel load prior to the flight, the lack of placards near the engine-monitoring instrument, and the pilot's reliance of the on-board engine-monitoring instrument instead of the fuel quantity gauges.

Jun 08, 2008 Bessemer, AL N45133 Minor substantial Failure of the left magneto for undetermined reasons resulting in a partial loss of engine power during takeoff.
Jun 19, 2007 Oceanside, CA N2144Q Minor substantial
The improper installation of the propeller governor (gasket) by maintenance personnel, which resulted in a oil exhaustion induced total loss of engine…

The improper installation of the propeller governor (gasket) by maintenance personnel, which resulted in a oil exhaustion induced total loss of engine power. Contributing to the accident was the lack of suitable terrain for the forced landing.

Apr 30, 2007 Perris, CA N177R Minor substantial a loss of engine power while in cruise flight due to an improperly installed magneto housing by the owner/pilot.
Oct 31, 2002 Marshall, AR N35866 Minor substantial The loss of engine power for undetermined reasons. A contributing factor was the lack of suitable terrain for the forced landing.
May 27, 2001 Pauma Valley, CA N8287G Minor substantial
The pilot's intentional flight into instrument meteorological conditions and failure to maintain clearance from terrain during an approach for landing…

The pilot's intentional flight into instrument meteorological conditions and failure to maintain clearance from terrain during an approach for landing under visual flight rules.

Apr 21, 2001 Seattle, WA N8283G Minor substantial
the reverse rigging of the aileron flight control system resulting in aileron deflections opposite that of the pilot's inputs which lead to an uncontr…

the reverse rigging of the aileron flight control system resulting in aileron deflections opposite that of the pilot's inputs which lead to an uncontrolled descent into the terrain. Factors include the pilot's failure to detect the misrigged ailerons during his pre-takeoff flight control check.

Jul 10, 1999 JASPER, AL N2619V Minor substantial
the pilot inadvertently became disoriented and misjudged his position on the runway/airport, which resulted in him turning the airplane too soon, and …

the pilot inadvertently became disoriented and misjudged his position on the runway/airport, which resulted in him turning the airplane too soon, and subsequently impacting with a tree. Factors in this accident were a loss of electrical power for undetermined reasons, resulting in the pilot not being able to activate the runway lights, and no visual cues due to a dark night.

Jul 05, 1999 QUINCY, CA N2175Q Minor substantial
the pilot's failure to attain and maintain an adequate airspeed for the existing wind conditions, and, his failure to abort the takeoff when it became…

the pilot's failure to attain and maintain an adequate airspeed for the existing wind conditions, and, his failure to abort the takeoff when it became apparent that the aircraft performance was not as anticipated. Factors in the accident were the tailwind and high density altitude conditions.

Jun 06, 1999 TIMMONSVILLE, SC N1982Q Minor substantial The loss of engine power due to the improper installation and in-flight separation of an engine cylinder.
Nov 19, 1997 TOMBALL, TX N88WC Minor substantial
The total loss of engine power resulting from the loss of oil and resultant seizure of a cylinder due to inadequate maintenance by maintenance personn…

The total loss of engine power resulting from the loss of oil and resultant seizure of a cylinder due to inadequate maintenance by maintenance personnel. A factor was the lack of suitable terrain for the forced landing and the low ceiling.

Jul 12, 1996 ROCKAWAY, NJ N8059G Minor substantial
The pilot's impairment of judgment and performance due to alcohol which led to his inadequate preflight of the aircraft and his inadequate inflight de…

The pilot's impairment of judgment and performance due to alcohol which led to his inadequate preflight of the aircraft and his inadequate inflight decision which resulted in fuel exhaustion and loss of engine power.

Oct 30, 1995 MADERA, CA N4110C Minor substantial
Fuel exhaustion due to the pilot's improper preflight planning and failure to ensure that adequate fuel was onboard to complete the flight. Darkness w…

Fuel exhaustion due to the pilot's improper preflight planning and failure to ensure that adequate fuel was onboard to complete the flight. Darkness was a related factor.

May 14, 1995 OAKLAND, CA N34938 Minor destroyed
The pilot's poor preflight planning/preparation by exceeding the airplane certificated maximum allowable takeoff gross weight and failure to abort the…

The pilot's poor preflight planning/preparation by exceeding the airplane certificated maximum allowable takeoff gross weight and failure to abort the takeoff in a timely manner. The ditch was a factor in this accident.

Mar 01, 1994 LONGMONT, CO N2181Q Minor substantial AN INADVERTENT STALL DUE TO IMPROPER PREFLIGHT AND THE PILOT'S FAILURE TO ADEQUATELY REMOVE ICE FROM THE AIRCRAFT. A FACTOR WAS AIRFRAME ICING.
Apr 16, 1993 CONCORD CITY, NC N44BG Minor substantial
THE FAILURE OF THE PILOT TO MAINTAIN CONTROL OF THE AIRCRAFT AND HIS DELAYED DECISION TO EXECUTE A GO AROUND. A FACTOR IN THE ACCIDENT WAS THE STRONG …

THE FAILURE OF THE PILOT TO MAINTAIN CONTROL OF THE AIRCRAFT AND HIS DELAYED DECISION TO EXECUTE A GO AROUND. A FACTOR IN THE ACCIDENT WAS THE STRONG GUSTY WIND CONDITION.

Apr 05, 1992 SCAPPOOSE, OR N52638 Minor destroyed THE LOSS OF ENGINE POWER, CAUSE UNDETERMINED. A FACTOR RELATING TO THE ACCIDENT WAS THE LACK OF SUITABLE TERRAIN FOR A FORCED LANDING.
Apr 13, 1991 SALUDA, SC N1960Q Minor substantial THE FLIGHT INSTRUCTOR DID NOT MAINTAIN THE PROPER ALTITUDE DURING THE SIMULATED FORCED LANDING.
Oct 14, 1990 DE FUNIAK SPGS, FL N52838 Minor substantial
THE LOOSE FUEL CAP AND FAILURE OF THE PILOT TO ASSURE THE AIRCRAFT WAS PROPERLY PREFLIGHTED, WHICH RESULTED IN FUEL SIPHONING AND SUBSEQUENT FUEL EXH…

THE LOOSE FUEL CAP AND FAILURE OF THE PILOT TO ASSURE THE AIRCRAFT WAS PROPERLY PREFLIGHTED, WHICH RESULTED IN FUEL SIPHONING AND SUBSEQUENT FUEL EXHAUSTION. FACTORS RELATED TO THE ACCIDENT WERE: FAULTY FUEL QUANTITY GAGES, THE PILOT'S DECISION TO FLY WITH KNOWN DEFICIENCIES IN THE AIRCRAFT, DARK NIGHT, LACK OF A SUITABLE LANDING AREA, AND THE VEHICLE.

Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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