Cessna 152 Safety Record
Complete NTSB accident and incident history. 2435 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jul 17, 1991 | SPRINGWATER, NY | N6489B | Incident | destroyed | THE ON GROUND COLLISION WITH TREES DURING A FORCED LANDING AFTER THE PILOT EXPERIENCED AN ENGINE FAILURE DUE TO A BROKEN EXHAUST VALVE. |
| Jul 14, 1991 | BENTON, TN | N757CB | Incident | substantial | A LOSS OF ENGINE POWER FOR UNDETERMINED REASONS. |
| Jul 09, 1991 | INDIAN SPRINGS, NV | N5533B | Minor | substantial |
FUEL EXHAUSTION DUE TO IMPROPER PREFLIGHT PLANNING, AND FAILURE TO REFUEL THE AIRCRAFT. FACTORS IN THE ACCIDENT WERE: 1) THE PILOT BECOMING LOST/DISO…FUEL EXHAUSTION DUE TO IMPROPER PREFLIGHT PLANNING, AND FAILURE TO REFUEL THE AIRCRAFT. FACTORS IN THE ACCIDENT WERE: 1) THE PILOT BECOMING LOST/DISORIENTED ; 2) THE DARK NIGHT CONDITIONS; 3) THE FAILURE OF THE PILOT TO SEEK HELP IN A TIMELY FASHION; AND 4) THE LOSS OF HIS EYEGLASSES WITH THE RESULTANT VISUAL PROBLEMS. |
| Jul 06, 1991 | WOODCHOPPER CRK, AK | N6276P | Incident | substantial |
ENGINE FAILURE DUE TO FUEL EXHAUSTION, THE PILOT'S INADEQUATE PREFLIGHT PLANNING AND THE UNSUITABLE TERRAIN. CONTRIBUTING TO THE ACCIDENT WAS THE PILO…ENGINE FAILURE DUE TO FUEL EXHAUSTION, THE PILOT'S INADEQUATE PREFLIGHT PLANNING AND THE UNSUITABLE TERRAIN. CONTRIBUTING TO THE ACCIDENT WAS THE PILOT'S LACK OF TOTAL EXPERIENCE. |
| Jul 04, 1991 | RUTLAND, VT | N69061 | Incident | substantial |
THE STUDENT PILOT IMPROPER RECOVERY FROM A BOUNCED LANDING WHICH RESULTED IN THE COLLAPSING OF THE NOSE GEAR. A FACTOR RELATED TO THE ACCIDENT WAS TH…THE STUDENT PILOT IMPROPER RECOVERY FROM A BOUNCED LANDING WHICH RESULTED IN THE COLLAPSING OF THE NOSE GEAR. A FACTOR RELATED TO THE ACCIDENT WAS THE STUDENT PILOT'S LACK OF TOTAL FLIGHT EXPERIENCE. |
| Jul 03, 1991 | RICHLAND, WA | N757MA | Incident | substantial | PARTIAL ENGAGEMENT OF THE PARKING BRAKE (LOCKING THE RIGHT BRAKE) FOR AN UNDETERMINED REASON. |
| Jun 25, 1991 | HUTTO, TX | N93097 | Incident | substantial | THE ENGINE FAILURE DUE TO CARBURETOR ICE. FACTORS WERE THE INSTRUCTOR'S IMPROPER USE OF CARBURETOR HEAT AND THE FOULED SPARK PLUGS. |
| Jun 21, 1991 | BROOKSVILLE, FL | N4733B | Incident | substantial |
FAILURE OF THE STUDENT PILOT TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRPLANE DURING THE LANDING ROLL. CONTRIBUTING TO THE ACCIDENT WAS HIS LACK OF TO…FAILURE OF THE STUDENT PILOT TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRPLANE DURING THE LANDING ROLL. CONTRIBUTING TO THE ACCIDENT WAS HIS LACK OF TOTAL EXPERIENCE. |
| Jun 18, 1991 | MURFREESBORO, TN | N25362 | Incident | substantial | STUDENT PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL DURING THE LANDING ROLL. |
| Jun 17, 1991 | OCEANSIDE, CA | N747CM | Incident | destroyed | FUEL EXHAUSTION DUE TO THE PILOT'S IMPROPER PREFLIGHT PLANNING. |
| Jun 15, 1991 | FOUNTAIN HILLS, AZ | N49627 | Incident | substantial |
THE FAILURE OF THE STUDENT PILOT AND INSTRUCTOR PILOT TO CORRECTLY CONFIGURE THE AIRCRAFT FOR THE ATTEMPTED GO AROUND. CONTRIBUTING TO THE ACCIDENT W…THE FAILURE OF THE STUDENT PILOT AND INSTRUCTOR PILOT TO CORRECTLY CONFIGURE THE AIRCRAFT FOR THE ATTEMPTED GO AROUND. CONTRIBUTING TO THE ACCIDENT WAS THE IMPROPER SUPERVISION OF THE FLIGHT BY THE FLIGHT INSTRUCTOR. |
| Jun 03, 1991 | PENSACOLA, FL | N65416 | Incident | substantial | THE PILOT-IN-COMMAND'S IMPROPER FLARE AND RECOVERY FROM A BOUNCED LANDING RESULTING IN A HARD LANDING AND COLLAPSE OF THE NOSE LANDING GEAR. |
| May 31, 1991 | HOLLAND, MI | N714UH | Incident | substantial |
THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE AIRPLANE DURING THE TOUCHDOWN AND LANDING ROLL ON A SOD RUNWAY. FACTORS IN THE ACCIDENT ARE THE UNEVEN …THE PILOT'S FAILURE TO MAINTAIN CONTROL OF THE AIRPLANE DURING THE TOUCHDOWN AND LANDING ROLL ON A SOD RUNWAY. FACTORS IN THE ACCIDENT ARE THE UNEVEN TERRAIN AT THE RUNWAY INTERSECTION, AND THE PILOT'S IMPROPER RECOVERY FROM A BOUNCED LANDING. |
| May 28, 1991 | HILLSDALE, MI | N5299B | Minor | substantial |
FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL DURING THE TAKEOFF GROUND RUN. A FACTOR ASSOCIATED WITH THE ACCIDENT IS THE PILOT'S LACK TOTAL E…FAILURE OF THE PILOT TO MAINTAIN DIRECTIONAL CONTROL DURING THE TAKEOFF GROUND RUN. A FACTOR ASSOCIATED WITH THE ACCIDENT IS THE PILOT'S LACK TOTAL EXPERIENCE. |
| May 23, 1991 | KNIGHTDALE, NC | N93002 | Incident | substantial |
THE STUDENT PILOT'S DELAY IN ABORTING THE TAKEOFF. THE PILOT'S CONTINUED OPERATION OF THE AIRPLANE WITH A KNOWN DISCREPANCY AND THE OPERATOR'S PREVIO…THE STUDENT PILOT'S DELAY IN ABORTING THE TAKEOFF. THE PILOT'S CONTINUED OPERATION OF THE AIRPLANE WITH A KNOWN DISCREPANCY AND THE OPERATOR'S PREVIOUS IMPROPER MAINTENANCE/INSPECTION OF THE PITOT/STATIC SYSTEM WERE FACTORS RELATED TO THE ACCIDENT. |
| May 23, 1991 | JACKSONVILLE, FL | N6495L | Incident | substantial | PARTIAL LOSS OF ENGINE POWER DUE TO FUEL EXHAUSTION DUE TO MISJUDGED FUEL CONSUMPTION CALCULATIONS. |
| May 22, 1991 | GREENVILLE, IL | N24394 | Incident | substantial | THE PILOT IN COMMAND'S MISJUDGMENT OF THE PROPER TOUCHDOWN POINT. AN ASSOCIATED FACTOR IS THE PILOT-IN-COMMAND NOT PERFORMING REMEDIAL ACTION. |
| May 18, 1991 | RICHMOND, CA | N6507H | Incident | substantial |
LOSS OF ENGINE POWER DUE TO CARBURETOR ICE. A FACTOR IN THE ACCIDENT WAS THE FAILURE OF THE INSTRUCTOR TO PROPERLY SUPERVISE THE CONDUCT OF THE FLIGH…LOSS OF ENGINE POWER DUE TO CARBURETOR ICE. A FACTOR IN THE ACCIDENT WAS THE FAILURE OF THE INSTRUCTOR TO PROPERLY SUPERVISE THE CONDUCT OF THE FLIGHT. |
| May 15, 1991 | NEWTONVILLE, NJ | N94512 | Incident | substantial |
PILOT FACTOR IN THAT THE STUDENT PILOT DELAYED ASKING FOR ASSISTANCE, AFTER BECOMING LOST UNTIL INSUFFICIENT FUEL WAS AVAILABLE TO MAKE AN AIRPORT. TH…PILOT FACTOR IN THAT THE STUDENT PILOT DELAYED ASKING FOR ASSISTANCE, AFTER BECOMING LOST UNTIL INSUFFICIENT FUEL WAS AVAILABLE TO MAKE AN AIRPORT. THIS RESULTED IN ENGINE FAILURE TO FUEL EXHAUSTION AND A SUBSEQUENT EMERGENCY LANDING IN ROUGH TERRAIN. |
| May 12, 1991 | YAZOO CITY, MS | N65619 | Incident | substantial |
POOR PLANNING DECISION BY THE STUDENT PILOT, IMPROPER FUEL CALCULATIONS, RESULTING IN FUEL EXHAUSTION DUE TO AN INADEQUATE FUEL SUPPLY. CONTRIBUTING T…POOR PLANNING DECISION BY THE STUDENT PILOT, IMPROPER FUEL CALCULATIONS, RESULTING IN FUEL EXHAUSTION DUE TO AN INADEQUATE FUEL SUPPLY. CONTRIBUTING TO THE ACCIDENT WAS OVERCONFIDENCE IN HIS OWN PERSONAL ABILITY BY THE STUDENT PILOT. |
| May 12, 1991 | BANNING, CA | N6258B | Incident | substantial | THE FAILURE OF THE PILOT TO UTILIZE THE PROPER TECHNIQUE TO RECOVER THE AIRPLANE FROM A BOUNCED LANDING. |
| May 11, 1991 | PONTIAC, MI | N69101 | Incident | substantial | RECOVERY FROM A BOUNCED LANDING WAS IMPROPER BY THE PILOT. FACTORS RELATED TO THE ACCIDENT WERE LACK OF RECENT EXPERIENCE BY THE PILOT. |
| May 01, 1991 | HAMPTON, GA | N6301L | Incident | substantial |
THE PILOT'S IMPROPER FLARE AND HIS FAILURE TO EXECUTE AN ABORT IN A TIMELY MANNER WHEN A SAFE LANDING WAS NOT POSSIBLE. FACTORS IN THE ACCIDENT WERE T…THE PILOT'S IMPROPER FLARE AND HIS FAILURE TO EXECUTE AN ABORT IN A TIMELY MANNER WHEN A SAFE LANDING WAS NOT POSSIBLE. FACTORS IN THE ACCIDENT WERE THE WET GRASS CONDITIONS AT THE AIRSTRIP, AND THE PILOT'S LACK OF RECENT TOTAL FLYING EXPERIENCE. |
| Apr 16, 1991 | OAK MEADOWS, FL | N4902H | Serious (2) | substantial |
THE FAILURE OF THE INSTRUCTOR PILOT TO MAINTAIN AN AIRSPEED ABOVE STALL SPEED RESULTING IN AN INADVERTENT STALL AT AN ALTITUDE THAT PRECLUDED RECOVERY…THE FAILURE OF THE INSTRUCTOR PILOT TO MAINTAIN AN AIRSPEED ABOVE STALL SPEED RESULTING IN AN INADVERTENT STALL AT AN ALTITUDE THAT PRECLUDED RECOVERY. CONTRIBUTING TO THE ACCIDENT WAS THE INSTRUCTOR PILOT'S POOR JUDGEMENT AND OSTENTATIOUS DISPLAY AT A LOW ALTITUDE. |
| Apr 10, 1991 | DURANT, OK | N116SS | Incident | substantial | THE PILOT'S FAILURE TO MAINTAIN PROPER ALIGNMENT DURING THE FLARE. |