Cessna 150L Safety Record
Complete NTSB accident and incident history. 464 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 29, 1998 | FREELAND, WA | N5867C | Incident | substantial |
Failure of the number two intake valve rocker arm in fatigue, and overload of the nose landing gear assembly. Factors include a ditch encountered du…Failure of the number two intake valve rocker arm in fatigue, and overload of the nose landing gear assembly. Factors include a ditch encountered during the forced landing. |
| Sep 29, 1998 | BONNERS FERRY, ID | N19427 | Incident | substantial |
Improper maintenance by an outsourcing facility which resulted in a lack of identification of scoring of the interior of the #3 cylinder rocker shaft …Improper maintenance by an outsourcing facility which resulted in a lack of identification of scoring of the interior of the #3 cylinder rocker shaft bosses. The scoring resulted in a fatigue fracture and subsequent permanent closure of both intake and exhaust valves. Contributing factors were the lack of a suitable landing site and trees. |
| Sep 19, 1998 | OROVILLE, CA | N19063 | Incident | substantial | Failure of the pilot to maintain proper clearance and subsequently striking a hangar door while taxiing to parking. |
| Aug 22, 1998 | CUMBERLAND, MD | N7513G | Incident | substantial | The pilot in command's improper recovery from a bounced landing. |
| Aug 09, 1998 | PHILIP, SD | N5413Q | Incident | substantial | the fuel exhaustion due to the pilot's inadequate preflight inspection. A factor was the soft field. |
| Jun 13, 1998 | TAFT, TX | N10519 | Incident | substantial |
The pilot's failure to ensure that there was adequate fuel for the planned flight on board the airplane during the preflight inspection which resulted…The pilot's failure to ensure that there was adequate fuel for the planned flight on board the airplane during the preflight inspection which resulted in a loss of engine power due to fuel exhaustion. A factor was the pilot's misjudgment of the glide distance during the forced landing which resulted in the airplane impacting objects short of the intended landing site. |
| May 31, 1998 | PEARLAND, TX | N19271 | Incident | substantial | The pilot's selection of the wrong runway/landing area. A factor was the lack of visual runway cues available to the pilot. |
| Mar 13, 1998 | CONWAY, AR | N21915 | Incident | substantial | The pilot's improper landing flare which resulted in a hard landing and her improper recovery procedures for a bounced landing. |
| Dec 14, 1997 | LITCHFIELD, MN | N18031 | Incident | destroyed |
the pilot's improper flare and improper recovery from a bounced landing, and his failure to maintain proper runway alignment during the attempted go-a…the pilot's improper flare and improper recovery from a bounced landing, and his failure to maintain proper runway alignment during the attempted go-around. Factors relating to the accident were: the crosswind condition, and the proximity of trees. |
| Nov 27, 1997 | CENTER VILLAGE, OH | N11350 | Incident | substantial | The student pilot's improper recovery from a bounced landing. |
| Mar 21, 1997 | NOGALES, AZ | N21993 | Incident | substantial | Loss of engine power due to fuel contamination resulting from the pilot's inadequate fuel storage and filtering procedures. |
| Sep 06, 1996 | HOPE, ME | N6632G | Incident | substantial |
inadequate preflight, by not refueling the airplane during an en route stop, which led to fuel exhaustion, loss of engine power, and a subsequent forc…inadequate preflight, by not refueling the airplane during an en route stop, which led to fuel exhaustion, loss of engine power, and a subsequent forced landing. |
| Jun 19, 1996 | SANFORD, FL | N11532 | Incident | substantial | failure of the pilot to maintain directional control of the airplane during the landing, which resulted in a ground swerve and subsequent nose over. |
| May 25, 1996 | MATAWAN, NJ | N10439 | Incident | substantial | the student pilot's improper flare and improper recovery from a bounced landing. The gusty wind condtion was a related factor. |
| Jan 13, 1996 | SUN CITY, FL | N18181 | Incident | substantial | The pilot's inadequate preflight planning, which resulted in fuel exhaustion. Darkness was a related factor. |
| Dec 29, 1995 | QUARTZITE, AZ | N1246Q | Incident | substantial |
the pilot's misjudgement of his distance and altitude relationship to the runway, which resulted in an undershoot and failure to achieve the proper to…the pilot's misjudgement of his distance and altitude relationship to the runway, which resulted in an undershoot and failure to achieve the proper touchdown point for landing. |
| Nov 19, 1995 | LANTANA, FL | N18201 | Incident | substantial | THE FAILURE OF THE PILOT-IN-COMMAND TO USE THE CHECKLIST AND TO SET THE PARKING BRAKES PRIOR TO ENGINE START. |
| Oct 26, 1995 | NORMAN, OK | N5350Q | Incident | substantial |
THE STUDENT PILOT'S IMPROPER RECOVERY FROM A BOUNCED LANDING AND THE FLIGHT INSTRUCTOR'S INADEQUATE SUPERVISION OF THE FLIGHT. FACTORS WERE THE GUSTY …THE STUDENT PILOT'S IMPROPER RECOVERY FROM A BOUNCED LANDING AND THE FLIGHT INSTRUCTOR'S INADEQUATE SUPERVISION OF THE FLIGHT. FACTORS WERE THE GUSTY WIND CONDITIONS AND THE STUDENT PILOT'S FAILURE TO OBTAIN AND MAINTAIN PROPER COMPENSATION FOR THE WIND CONDITIONS. |
| Aug 10, 1995 | OPA LOCKA, FL | N19561 | Incident | substantial | The pilot-in-command's improper use of flaps during an attempted go-around. |
| Aug 05, 1995 | PICAYUNE, MS | N18679 | Incident | substantial | LOSS OF ENGINE POWER DUE TO UNDETERMINED REASONS. |
| Jul 02, 1995 | HOLLY RIDGE, NC | N28445 | Incident | substantial | the pilot diverted his attention and failed to maintain clearance from obstacles. |
| Jun 11, 1995 | LEVELLAND, TX | N10964 | Incident | minor |
THE FAILURE OF THE PILOT OF THE OTHER AIRCRAFT TO MAINTAIN CLEARANCE DURING A FORMATION FLIGHT. A FACTOR WAS THE LACK OF EXPERIENCE IN THE TYPE OF OPE…THE FAILURE OF THE PILOT OF THE OTHER AIRCRAFT TO MAINTAIN CLEARANCE DURING A FORMATION FLIGHT. A FACTOR WAS THE LACK OF EXPERIENCE IN THE TYPE OF OPERATION. |
| Mar 03, 1995 | JEFFERSON, GA | N1321Q | Incident | substantial | THE LOSS OF ENGINE POWER BECAUSE OF STICKING VALVES. A FACTOR WAS THE CONTINUOUS USE OF AN IMPROPER FUEL GRADE. |
| Dec 27, 1994 | NORTH LAS VEGAS, NV | N7446G | Incident | substantial | the pilot's improper in-flight planning and decisions, and his failure to initiate remedial actions in a timely fashion. |
| Oct 30, 1994 | CRYSTAL RIVER, FL | N19264 | Incident | substantial | A PARTIAL LOSS OF ENGINE POWER FOR UNDETERMINED REASONS. THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING WAS A FACTOR. |