Bell 47 Safety Record

Complete NTSB accident and incident history. 744 events recorded from 1982 to 2026.

744

All Events

391

Incidents

169

Minor

96

Serious

84

Fatal (106 fatalities)

Date Location Reg# Severity Damage Probable Cause
Nov 15, 1995 JASPER, FL N4702S Incident substantial
IMPROPER MAINTENANCE AND INSPECTION OF THE CARBURETOR SYSTEM BY MAINTENANCE PERSONNEL DURING THE LAST ANNUAL INSPECTION WHICH RESULTED IN A PARTIAL LO…

IMPROPER MAINTENANCE AND INSPECTION OF THE CARBURETOR SYSTEM BY MAINTENANCE PERSONNEL DURING THE LAST ANNUAL INSPECTION WHICH RESULTED IN A PARTIAL LOSS OF ENGINE POWER DUE TO CARBURETOR ICE. CONTRIBUTING TO THE ACCIDENT WERE: THE PILOT'S FAILURE TO PERFORM AN ADEQUATE PREFLIGHT AND ENGINE RUN-UP, AND THE CARBUETOR ICING CONDITIONS.

Nov 02, 1995 PACIFIC OCEAN, PO N99138 Incident destroyed
failure of the pilot to maintain lateral control of the helicopter, while hovering in preparation for a precautionary landing next to a ship at sea. …

failure of the pilot to maintain lateral control of the helicopter, while hovering in preparation for a precautionary landing next to a ship at sea. Factors relating to the accident were: the passenger's premature evacuation from the helicopter, and the resultant lateral imbalance of the helicopter as the passenger jumped.

Sep 21, 1995 UNION CITY, TN N616X Incident substantial Failure of a #4 connecting rod bolt, which resulted in engine stoppage and a forced landing.
Sep 10, 1995 YUMA, AZ N7942J Incident substantial
the failure of the pilot and company maintenance personnel to detect a crack in the clevis ears during the required daily inspection and the recent an…

the failure of the pilot and company maintenance personnel to detect a crack in the clevis ears during the required daily inspection and the recent annual inspection. A factor in the accident was the improper welding and stress relief procedure used to assemble the components, which induced high residual stresses in the clevis ears and led to fatigue cracking of the part.

Aug 22, 1995 SIDNEY, OH N9115R Incident substantial
the student pilot's abrupt touchdown while landing in a field. Related factors are the student pilot's failure to attain the proper descent rate duri…

the student pilot's abrupt touchdown while landing in a field. Related factors are the student pilot's failure to attain the proper descent rate during the approach to landing, and the flight instructor's inadequate supervision of the student.

Jul 31, 1995 MONTROSE, GA N6145C Incident substantial The pilot's inadequate preflight planning and visual lookout.
Jun 19, 1995 ELKHORN, WI N470RA Incident substantial
loss of power as a result of an intake valve failure due to improper maintenance performed during the major engine overhaul, and pilot misjudgment of …

loss of power as a result of an intake valve failure due to improper maintenance performed during the major engine overhaul, and pilot misjudgment of the flare during autorotation.

Jun 18, 1995 COALINGA, CA N7923J Incident destroyed
clutch slippage for undetermined reasons. A factor in the accident was the helicopter's low above ground altitude, which limited the pilot's time and…

clutch slippage for undetermined reasons. A factor in the accident was the helicopter's low above ground altitude, which limited the pilot's time and ability to recover main rotor rpm.

Jun 18, 1995 BAKERSFIELD, CA N73260 Incident substantial the pilot's failure to maintain adequate lateral clearance from the irrigation standpipe while applying chemicals to a field.
May 30, 1995 FALFURRIAS, TX N1502L Incident substantial
INADVERTENT INSTALLATION OF AN UNAPPROVED PART (TAIL ROTOR GEAR/DRIVE ASSEMBLY), THAT BECAME EXCESSIVELY WORN SINCE IT DID NOT CONFORM TO THE MANUFACT…

INADVERTENT INSTALLATION OF AN UNAPPROVED PART (TAIL ROTOR GEAR/DRIVE ASSEMBLY), THAT BECAME EXCESSIVELY WORN SINCE IT DID NOT CONFORM TO THE MANUFACTURER'S SPECIFICATION, RESULTING IN FAILURE OF THE ASSOCIATED TAIL ROTOR BEARING (ALSO AN UNAPPROVED PART), LOSS OF CONTINUITY (DISCONNECT) OF THE TAIL ROTOR DRIVE SYSTEM, AND A FORCED AUTOROTATION INTO AN AREA WITH TREES.

Mar 17, 1995 HARMON FIELD, N6569H Incident substantial an engine failure due to oil exhaustion from a missing oil pressure relief valve as the result of an improper maintenance inspection.
Feb 07, 1995 CHINA LAKE, CA N73240 Incident substantial the pilot's misjudgement of the clearance between the main rotor and a tree while maneuvering at low altitude to herd animals.
Sep 23, 1994 MOORE HAVEN, FL N30JJ Incident destroyed
The pilot-in-command's failure to maintain a visual lookout while maneuvering on a swath run, resulting in an in-flight collision with wires, and subs…

The pilot-in-command's failure to maintain a visual lookout while maneuvering on a swath run, resulting in an in-flight collision with wires, and subsequent in-flight collision with terrain.

Sep 13, 1994 HAZEL GREEN, AL N908B Incident substantial UNDETERMINED.
Aug 26, 1994 LAKE CITY, MN N19JM Incident substantial
THE LOSS OF LIFT RESULTING FROM THE PILOT'S FAILURE TO MAINTAIN ROTOR RPM DURING AN AERIAL APPLICATION TURN. THE POWER AVAILABLE FROM THE ENGINE WAS L…

THE LOSS OF LIFT RESULTING FROM THE PILOT'S FAILURE TO MAINTAIN ROTOR RPM DURING AN AERIAL APPLICATION TURN. THE POWER AVAILABLE FROM THE ENGINE WAS LESS THAN THAT REQUIRED TO REGAIN THE LOST ROTOR RPM.

Aug 11, 1994 SARGEANT, MN N64292 Incident substantial
the pilot's failure to maintain clearance from a transmission wire during an agricultural spray run. A factor in the accident is the transmission wire…

the pilot's failure to maintain clearance from a transmission wire during an agricultural spray run. A factor in the accident is the transmission wire.

Jul 30, 1994 SCOTTSDALE, AZ N6749D Incident substantial THE PILOT'S FAILURE TO REFUEL APPROPRIATELY, THE ALTITUDE AND AIRSPEED AT THE TIME THE ENGINE STOPPAGE OCCURRED WERE FACTORS IN THE ACCIDENT.
Jun 04, 1994 TULSA, OK N2831B Incident substantial THE PILOT'S FAILURE TO MAINTAIN ROTOR RPM, HIS DELAYED LANDING FLARE, AND THE IMPROPER TOUCHDOWN.
Jun 02, 1994 CHINO, CA N14412 Incident substantial loss of aircraft control due to the pilot's failure to correctly configure the hydraulic system prior to takeoff.
May 18, 1994 SULPHUR, OK N933B Incident substantial THE LOSS OF ENGINE POWER DUE TO THE FAILURE OF AN ENGINE ACCESSORY OIL PUMP GEAR. A FACTOR WAS THE LACK OF SUITABLE TERRAIN FOR THE AUTOROTATION.
Apr 27, 1994 SPRINGFIELD, MO N46DH Incident substantial the pilot-in-command misjudging the autorotation and improper use of collective.
Apr 17, 1994 YUMA, AZ N304JP Incident substantial an uncommanded engine deceleration to idle due to the improper installation of the throttle arm on the carburetor shaft.
Apr 13, 1994 WILLCOX, AZ N5827U Incident substantial ENGINE POWER LOSS DUE TO FUEL CONTAMINATION AS A RESULT OF INADEQUATE INSPECTION OF THE FUEL AND FUEL SYSTEM.
Apr 12, 1994 TROUTDALE, OR N2865B Incident substantial
THE INSTRUCTOR PILOT'S INADEQUATE REMEDIAL ACTION. FACTORS INCLUDE THE DUAL STUDENT'S LACK OF EXPERIENCE, AND HIS FAILURE TO MAINTAIN DIRECTIONAL CONT…

THE INSTRUCTOR PILOT'S INADEQUATE REMEDIAL ACTION. FACTORS INCLUDE THE DUAL STUDENT'S LACK OF EXPERIENCE, AND HIS FAILURE TO MAINTAIN DIRECTIONAL CONTROL. ANOTHER FACTOR WAS UNFAVORABLE, GUSTY WINDS.

Mar 05, 1994 AURORA, MO N6711D Incident substantial THE DUAL STUDENTS INADEQUATE FLARE AND THE PILOT IN COMMAND'S (FLIGHT INSTRUCTOR) DELAYED REMEDIAL ACTION.
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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