Bell 47 Safety Record
Complete NTSB accident and incident history. 744 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Mar 30, 2014 | Oglesby, TX | N147WT | Incident | substantial |
Maintenance personnel’s failure to safety wire the throttle control adapter per maintenance instructions when the carburetor was replaced and to detec…Maintenance personnel’s failure to safety wire the throttle control adapter per maintenance instructions when the carburetor was replaced and to detect that the adapter was not safety wired during the annual inspection, which resulted in the throttle control disconnecting and subsequent loss of engine control. |
| Feb 18, 2014 | Greenfield, CA | N715BH | Incident | substantial | The pilot's failure to maintain clearance from a power pole during low-altitude maneuvering flight. |
| Sep 11, 2013 | King City, CA | N7836S | Incident | substantial |
The failure of the helicopter’s center frame tube due to a fatigue crack and corrosion originating from a welded surface. Contributing to the accident…The failure of the helicopter’s center frame tube due to a fatigue crack and corrosion originating from a welded surface. Contributing to the accident was maintenance personnel’s inadequate inspection of the helicopter during its most recent 100-hour inspection. |
| Aug 06, 2013 | Vinton, IA | N83702 | Incident | substantial |
The pilot's operation of the helicopter at high gross weight and high density altitude while still in ground effect, which reduced the efficiency of t…The pilot's operation of the helicopter at high gross weight and high density altitude while still in ground effect, which reduced the efficiency of the rotor system and the amount of lift produced, which resulted in a collision with terrain. Contributing to the accident was the pilot's decision to continue the flight after the first indication of reduced performance. |
| Jun 28, 2013 | Lake Ozark, MO | N78900 | Incident | substantial |
The improper rebuild and maintenance of the helicopter and inadequate subsequent inspections, which resulted in undetected fuel contamination and a su…The improper rebuild and maintenance of the helicopter and inadequate subsequent inspections, which resulted in undetected fuel contamination and a subsequent total loss of engine power during cruise flight. |
| Aug 14, 2012 | Flandreau, SD | N444EH | Incident | substantial | A malfunction of the helicopter’s throttle system, which resulted in a loss of engine power during cruise flight. |
| Jul 09, 2012 | Treynor, IA | N2919W | Incident | substantial | The pilot’s improper fuel management, which resulted in a loss of engine power due to fuel exhaustion. |
| Nov 08, 2011 | San Diego, CA | N4251A | Incident | substantial |
The flight instructor's inadequate supervision of the student pilot during a simulated autorotation and the pilots’ failure to use carburetor heat whi…The flight instructor's inadequate supervision of the student pilot during a simulated autorotation and the pilots’ failure to use carburetor heat while operating at reduced engine power while in carburetor icing conditions, which resulted in a loss of engine power. |
| Aug 14, 2011 | Los Banos, CA | N475AL | Incident | substantial |
The pilot’s inadequate preflight, and contamination of both the engine compressor section and the main rotor blades, which resulted in reduced perform…The pilot’s inadequate preflight, and contamination of both the engine compressor section and the main rotor blades, which resulted in reduced performance of the engine and rotor system. |
| Jul 31, 2011 | Porterville, CA | N6260C | Incident | substantial | The pilot's decision to takeoff in a tailwind condition, and his subsequent failure to attain sufficient lift during the takeoff. |
| Jul 27, 2011 | Nicolett, MN | N7578 | Incident | substantial | The pilot's failure to maintain control of the helicopter while maneuvering during an aerial application flight. |
| Jul 20, 2011 | Watsonville, CA | N1375X | Incident | substantial | The pilot's failure to maintain clearance from a pole while maneuvering during an aerial application flight. |
| Jun 18, 2011 | Montgomery City, MO | N24HM | Incident | substantial |
A loss of control during the precautionary landing, which resulted in inadvertent contact between the main rotor and the tailboom. Contributing to the…A loss of control during the precautionary landing, which resulted in inadvertent contact between the main rotor and the tailboom. Contributing to the accident was the overloaded condition. |
| Sep 26, 2010 | Gaston, OR | N7860S | Incident | substantial | The pilot's failure to maintain tail rotor clearance while landing on a transport trailer positioned on an uneven surface. |
| Jun 13, 2010 | Plymouth, MI | N47WK | Incident | substantial | The pilot's failure to use carburetor heat, which led to carburetor icing and a loss of engine power following takeoff. |
| Jun 08, 2010 | Shaw Island, WA | N7069J | Incident | substantial | The passenger's inadvertent movement of the mixture control during climb, resulting in a loss of engine power. |
| Oct 02, 2009 | Dorrance, PA | N74004 | Incident | substantial | A total loss of engine power due to fuel exhaustion for undetermined reasons. |
| Aug 11, 2009 | Covert, MI | N9526 | Incident | substantial | A loss of engine power due to fuel starvation as a result of blocked fuel vents. |
| Jul 08, 2009 | Turlock, CA | N6768D | Incident | substantial | The pilot's failure to maintain rotor RPM while maneuvering at a low altitude. |
| Oct 11, 2008 | Florence, AZ | N8567F | Incident | substantial |
The pilot’s inadequate compensation for a wind shift encountered during the landing approach, which resulted in a hard landing and rollover. Contribu…The pilot’s inadequate compensation for a wind shift encountered during the landing approach, which resulted in a hard landing and rollover. Contributing to the accident was the encounter with the wind shift. |
| Aug 14, 2008 | Kenyon, MN | N47AH | Incident | substantial | The pilot's inadequate preflight planning which resulted in the helicopter settling with power. |
| Jul 24, 2008 | Lafetyette, IN | N4029G | Incident | substantial |
The loss of engine power during an aerial application flight due to a fatigue fracture of the carburetor heat control valve spring and the inadequate …The loss of engine power during an aerial application flight due to a fatigue fracture of the carburetor heat control valve spring and the inadequate maintenance inspection by the pilot/mechanic. An additional cause was the low altitude of the operation. |
| Jul 15, 2008 | Shafter, CA | N1390X | Incident | substantial |
The pilot's failure to maintain adequate altitude while maneuvering. Contributing factors were the failure of the helicopter's lights during the night…The pilot's failure to maintain adequate altitude while maneuvering. Contributing factors were the failure of the helicopter's lights during the night flight and the effect of that failure on the pilot's visual perception. |
| Jul 01, 2008 | Mullen, NE | N8468E | Incident | substantial |
The plot's distraction with the chemical load resulting the failure to maintain control of the helicopter. A factor was no suitable terrain for landi…The plot's distraction with the chemical load resulting the failure to maintain control of the helicopter. A factor was no suitable terrain for landing. |
| Jun 01, 2008 | Carrollton, OH | N74898 | Incident | substantial | The airframe vibration for an undetermined reason. |