1974 Cessna 172M
Single Engine Piston
Aircraft Details
Seller reportedAvionics & Equipment
IFRDual Garmin G5 electronic flight display ( Attitude indicator HSI ) Appareo Stratus ESG ADSB in out transponder Garmin G430W Garmin GMA 340 audio panel KX 175B TSO secondary radio/nav
Description
This stunning 1974 Cessna 172 N1908F has just landed on the market. N1908F is the perfect time builder, trainer, and cross country machine. Equipped with dual Garmin G5's, a Garmin 430W, ADSB in Out this aircraft truly sets the bar high for its category. Sporting a fresh annual completed by trusted local mechanics it is ready to depart on its new adventure to train the next generation of aviators. If interested please contact the seller for more information on this stunning aircraft.
Interior
Interior is in good condition rated 7/10
Description and equipment details provided by the seller. AeroGurus does not verify seller-provided information.
Price Comparison 1 active offer
| Source | Price | Location | Listed | Days on Market | Status | Action |
|---|---|---|---|---|---|---|
|
Hunter Melton
trade-a-plane.com
|
$142,500
|
Matthews, NC | Apr 13, 2026 | — | Active |
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AeroGurus Data & Analysis
Independent data from FAA, NTSB, and market analysis
About This Cessna 172M
This 1974 Cessna 172M (N1908F) is a 4-seat single engine piston with 9,170 hours on the airframe. There are currently 42 172M aircraft listed for sale with asking prices ranging from $59,819 to $299,000. This aircraft is priced below the market average at $142,500.
The 172M cruises at 122 kts (226 km/h) with a range of 640 nm (1,185 km) — ideal for short hops and local flights. Service ceiling of 14,000 ft allows operation above most weather.
Operating costs: Fuel burn is 8.6 GPH (33 L/h), which at current Jet-A prices (~$5.50/gal) means approximately $47/hr in fuel alone. Total variable cost including maintenance reserves is approximately $130/hr. Annual fixed costs (hangar, insurance, crew, annual inspection) average $18,000. With 9,170 hours on the airframe, this aircraft has exceeded TBO (2,000 hrs) — verify engine status and overhaul reserve.
NTSB records show 0 incidents for this airframe — a clean safety record. Mechanics have filed 10 service difficulty reports for this type — common maintenance items to discuss during pre-buy.
Pre-Purchase Checklist
Cessna 172M — Model Specs
Model specificationStandard specs for this model. Actual aircraft may differ.
Estimated Cost of Ownership
AeroGurus estimateCESSNA 172
AeroGurus estimates based on industry averages for the CESSNA 172. Actual costs vary by location, usage, maintenance history, and configuration. Not a financial quote.
Ownership & Registration
FAA registration data pending for N1908F.
Location & Ownership
Title Status
No FAA title records
Available for US-registered aircraft only
Source: FAA Aircraft Registry, FAA Civil Aviation Registry (DocIndex). Title data may be delayed. Always verify with an aviation attorney before purchase.
Safety Record
NTSB safety data coming soon.
We'll check N1908F against the NTSB accident database.
Service Difficulty Reports — Cessna 172M
SDRs are reports filed by mechanics about problems found during maintenance. 10 recent reports for this aircraft type.
POSITION # 1 &2 CYLINDER EXHAUST PORT CRACK FROM THE INBOARD EXHAUST STUD EXTENDING TO THE BACK OF THE PORT. CRACK VISIBLE THROUGH THE FINS. SUPERIOR CYLINDERS PN: SL32006W-A1 SERIAL NUMBER 326W000003625 & 326W000003623.
STATIC CONDENSATION BULB P/N S-1258-1 FOUND SEPARATED FROM AN 1/8 PIPE BY PIPE 90 DEGREE FITTING. THESE CONDENSATION BULBS ARE OF VERY CHEAP PLASTIC AND ARE FAMOUS FOR LEAKING RIGHT OUT OF THE BOX. THERE SEEMS TO BE NO OTHER PART OF BETTER QUALITY. I...
THE BATTERY BOX FOR THE LEAD ACID BATTERY INTERFERES WITH THE LEFT MAGNETO HARNESS AND CHAFES THE HARNESS LEADS OVER TIME. THE INBOARD , FORWARD CORNER IS THE POINT OF CONTACT. I HAVE SEEN THIS SITUATION IN MANY 172S. ELECTRONIC MAGNETOS LIKE THE SUR...
ON APPROACH CARBURETOR HEAT WAS APPLIED AND THE ENGINE IMMEDIATELY LOST POWER BUT DID NOT STOP RUNNING. THE PILOT ATTEMPTED TO DE-SELECT THE CARBURETOR HEAT AND THE LOSS OF POWER PERSISTED. THE AIRCRAFT WAS ABOUT 2300 FEET MSL AND 2 NM FROM THE RUNWA...
ACFT RETURNED TO BASE DUE TO VIBRATION AT 300FT ON 2/8/25. PILOT REPORTED ENGINE STARTED SHAKING SIGNIFICANTLY. HE PULLED CARB HEAT HOT SAW NO CHANGE. TOLD TOWER HE WAS LANDING. CARB HEAT SYSTEM WAS INSPECTED WITH NO DEFECTS FOUND. CARB WAS REPLA...
REMOVED AND REPLACED RH MAGNETO DUE TO 500 HOUR OVERHAUL LIMIT. NEW MAGNETO INSTALLED FOR 78.2 HOURS BEFORE A FLIGHT WAS CANCELLED DUE TO EXCESSIVE VIBRATION AND HIGH MAG DROP ON RH SIDE AT PRE-RUN. ATTEMPTED TO TIME RH MAGNETO TO ENGINE. POINTS APPE...
TOTAL INTERNAL CRANKSHAFT FAILURE AT CHEEK BETWEEN #3 AND #4 CONNECTING ROD JOURNALS CAUSING CRANKCASE TO COMPLETELY SEPARATE IN THE CENTER. CRACK APPEARS TO HAVE STARTED IN THE REAR THRUST RADIUS OF #3 CONNECTING ROD JOURNAL. PILOT HAD REPORTED ...
DURING INSPECTION FOR ROUGH RUNNING ENGINE, PERFORMED SB388C (EXHAUST VALVE GUIDE INSPECTION) & FOUND 3EA ROCKER ARMS P/N 17F19357 & 3EA PUSH RODS P/N 15F19957-10 WITH MECHANICAL DAMAGE (HEAVY SCUFF - SCORING). ROCKER ARMS & PUSH RODS TSN: 147.9. PRE...
LYCOMING FACTORY OVERHAULED O-320-D2J, S/N L-17060-39E. DURING ROUTINE MX, SB388C (EXHAUST VALVE GUIDE INSP.) FOUND 4EA PUSH RODS P/N 15F28835-10, 2EA PUSH RODS P/N 15F28835-09, 6EA ROCKER ARMS P/N17F19357, 6EA SOCKETS P/N 15B21319 & 6EA LIFTERS P/N ...
LYCOMING FACTORY REBUILT - O-320-D2J, S/N RL-20892-39E. DURING ROUTINE MX. SB388C (EXHAUST VALVE GUIDE INSPECTION) FOUND 3EA HYDRUALIC TAPPETS P/N 15B21319, 3EA HYDRAULIC LIFTERS P/N 15B26066, 3EA ROCKER ARMS P/N 17F19357, 2EA PUSH RODS P/N 15F28835-...
Source: FAA Service Difficulty Reporting System. Shows maintenance issues reported by mechanics for this aircraft type.