Rotorway EXEC Safety Record
Complete NTSB accident and incident history. 49 events recorded from 1984 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Apr 01, 2002 | Chandler, AZ | N21901 | Serious (1) | substantial | The tail rotor drive system failure as a result of incorrect installation procedures by the manufacturer's personnel. |
| Jul 23, 2000 | CIRCLEVILLE, OH | N651GE | Serious (1) | substantial |
Pilot's improper decision to depart a confined area with two people onboard, which resulted in a loss of rotor RPM and collision with a utility pole a…Pilot's improper decision to depart a confined area with two people onboard, which resulted in a loss of rotor RPM and collision with a utility pole and wires. |
| Jul 16, 2000 | TOOELE, UT | N6399L | Minor | substantial |
The pilot's inadequate weather evaluation, which resulted in a downwind landing, and his failure to maintain aircraft control. A factor was the tailw…The pilot's inadequate weather evaluation, which resulted in a downwind landing, and his failure to maintain aircraft control. A factor was the tailwind. |
| May 13, 2000 | ITHACA, MI | N962WM | Fatal (1) | destroyed | the door separation for undetermined reasons and the foreign object damage due to the door impact to the tailboom and tail rotor drive system. |
| Apr 06, 2000 | CHANDLER, AZ | N21901 | Incident | substantial |
The inadequate maintenance inspection of the secondary shaft which resulted in its fatigue failure that emanated from a corroded circumferential score…The inadequate maintenance inspection of the secondary shaft which resulted in its fatigue failure that emanated from a corroded circumferential score mark. A factor was the fence that the pilot flared to avoid, resulting in a hard landing. |
| Jan 04, 2000 | CHANDLER, AZ | N89678 | Incident | substantial | the fatigue fracture and separation of the secondary drive shaft, which resulted from the manufacturer's inadequate quality control process. |
| Dec 17, 1999 | GEORGETOWN, IN | N990JR | Incident | substantial |
the pilot's failure to maintain control of the helicopter. Factors associated with the accident were the gusty tailwind condition and the low altitude…the pilot's failure to maintain control of the helicopter. Factors associated with the accident were the gusty tailwind condition and the low altitude at which the helicopter was hovering. |
| Jun 05, 1998 | NEW PORT RICHEY, FL | N162WM | Incident | substantial | The pilot's improper use of the collective. Contributing to the accident was pilot fatigue due to lack of sleep. |
| Jun 04, 1998 | LEXINGTON, NE | N132RS | Incident | substantial |
An improper autorotation by the pilot in command. Factors contributing to this accident were the accumulation of ice in the carburetor resulting in a…An improper autorotation by the pilot in command. Factors contributing to this accident were the accumulation of ice in the carburetor resulting in a total loss of engine power, and the soft terrain. |
| Jul 16, 1996 | ANCHORAGE, AK | N9297H | Fatal (1) | destroyed |
the pilot's excessive control inputs and the lack of familiarity with the helicopter. A factor associated with the accident was the pilot's failure to…the pilot's excessive control inputs and the lack of familiarity with the helicopter. A factor associated with the accident was the pilot's failure to follow the prescribed operating limitations. |
| Jun 10, 1996 | GRETNA, VA | N7182Z | Incident | destroyed |
failure of the bearing assembly shaft insert inside the main rotor shaft. Related factors are the jammed rotorcraft flight control which restricted t…failure of the bearing assembly shaft insert inside the main rotor shaft. Related factors are the jammed rotorcraft flight control which restricted the pilot's ability to control the helicopter and resulted in a hard touchdown. |
| May 22, 1996 | CHANDLER, AZ | N89678 | Incident | substantial | a loss of engine power due to a failed piston and piston ring in a critical phase of flight. |
| Dec 28, 1993 | SCOTTSDALE, AZ | N7456T | Minor | destroyed |
A failure of the pilot-in-command to adequately conduct a preflight inspection and properly secure a fuselage cowling panel that struck a tail rotor b…A failure of the pilot-in-command to adequately conduct a preflight inspection and properly secure a fuselage cowling panel that struck a tail rotor blade, resulting in a subsequent failure of the tail rotor drive system. Factors in this accident were an in-flight separation of the cowling panel, and the inability of the pilot to effect directional control of the helicopter. |
| Dec 08, 1993 | CHANDLER, AZ | N89678 | Minor | substantial |
THE FLIGHT INSTRUCTOR'S FAILURE TO PROPERLY FOLLOW THE AIRCRAFT BALLASTING PROCEDURES THAT RESULTED IN A LOSS OF CONTROL WHEN THE HELICOPTER'S CENTER …THE FLIGHT INSTRUCTOR'S FAILURE TO PROPERLY FOLLOW THE AIRCRAFT BALLASTING PROCEDURES THAT RESULTED IN A LOSS OF CONTROL WHEN THE HELICOPTER'S CENTER OF GRAVITY LIMITS WERE EXCEEDED. INADEQUATE SUPERVISION OF THE TRAINING FLIGHT WAS A FACTOR IN THE ACCIDENT. |
| Dec 31, 1992 | CHANDLER, AZ | N43385 | Incident | destroyed | AN ENGINE COMPARTMENT FIRE FOR UNDETERMINED REASONS. |
| Sep 08, 1991 | PHOENIX, AZ | N7456T | Fatal (1) | substantial | UNDETERMINED. |
| Sep 02, 1989 | PALMYRA, VA | N27TB | Serious (2) | destroyed | INADEQUATE PREFLIGHT BY THE PILOT, AND FUEL EXHAUSTION DUE TO AN INADEQUATE SUPPLY OF FUEL. |
| May 29, 1989 | ROSWELL, GA | N7043T | Incident | substantial | THE PILOTS IMPROPER USE OF THE TAIL ROTOR CONTROLS WHILE IN A HOVER. ADDING TO THIS WAS THE PILOTS TOTAL LACK OF EXPERIENCE OPERATING HELICOPTERS. |
| Jan 09, 1988 | COLORADO SPRING, CO | N7007B | Incident | destroyed | Investigation pending |
| Jul 19, 1987 | HIGHRIDGE, MO | N275FS | Serious (1) | substantial | Investigation pending |
| Apr 28, 1987 | GERALD, MO | N4891H | Incident | substantial | Investigation pending |
| Oct 15, 1985 | EL MONTE, CA | N2071Z | Incident | substantial | Investigation pending |
| Feb 27, 1985 | BETHANY, OK | N3071 | Incident | substantial | Investigation pending |
| Jul 11, 1984 | CAMBRIDGE, WI | N2993P | Incident | destroyed | Investigation pending |