Robinson R44 Safety Record
Complete NTSB accident and incident history. 366 events recorded from 1993 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Sep 30, 2018 | Westminster, MD | N440SH | Incident | substantial |
The pilot's attempt to move the helicopter from a sloped surface after an overspeed event, which resulted in a loss of helicopter control and impact w…The pilot's attempt to move the helicopter from a sloped surface after an overspeed event, which resulted in a loss of helicopter control and impact with a car. The overspeed event resulted from misrouted and damaged wiring in the magneto, which subsequently resulted in errant and random signals to the governor. |
| Sep 18, 2018 | Wahiawa, HI | N632NV | Incident | substantial |
Loss of oil in flight as a result of a loose oil filter adapter which resulted in the pilot initiating an immediate landing to an open field. Contribu…Loss of oil in flight as a result of a loose oil filter adapter which resulted in the pilot initiating an immediate landing to an open field. Contributing to the accident was the pilot's manipulation of the throttle that led to a reduction in rotor rpm, which resulted in his inability to perform a normal landing. |
| Aug 30, 2018 | Girdwood, AK | N99645 | Incident | substantial | The fisherman's fishing rod striking the helicopter’s rotating main rotor disk during loading. |
| Jul 29, 2018 | Bettles, AK | N744AK | Incident | substantial |
Maintenance personnel's application of insufficient preload on the attachment hardware for the idler gear shaft during engine overhaul, which resulted…Maintenance personnel's application of insufficient preload on the attachment hardware for the idler gear shaft during engine overhaul, which resulted in the dismounting of the idler gear shaft assembly due to wear and deformation and the subsequent total loss of engine power. Contributing to the accident was a mechanic's failure to identify metallic particles contained in the oil filter element at the most recent 100-hour inspection. |
| Jul 10, 2018 | Rulo, NE | N144DJ | Incident | substantial |
The pilot's improper collective application, which resulted in low rotor rpm during the takeoff climb and a subsequent ground collision. Contributing …The pilot's improper collective application, which resulted in low rotor rpm during the takeoff climb and a subsequent ground collision. Contributing to the accident was the pilot’s self-induced pressure to complete the operation. |
| Jul 09, 2018 | Okawville, IL | N944DC | Incident | substantial |
The pilot's improper preflight weight and balance calculation, which resulted in his operating the helicopter over its maximum gross takeoff weight an…The pilot's improper preflight weight and balance calculation, which resulted in his operating the helicopter over its maximum gross takeoff weight and in its subsequent failure to climb. |
| Apr 20, 2017 | Orlando, FL | N899GB | Incident | substantial |
A partial failure of the helicopter's engine tachometer due to the separation of one of the magnet assemblies and engine roughness, which precipitated…A partial failure of the helicopter's engine tachometer due to the separation of one of the magnet assemblies and engine roughness, which precipitated the pilot’s initiation of an off-airport autorotation, during which he applied improper aft cyclic flight control input, which was contrary to the Pilot’s Operating Handbook. The reason for the reported engine roughness could not be determined during postaccident examination and engine test-runs. |
| Aug 26, 2016 | Kailua/Kona, HI | N74805 | Incident | substantial |
An on-ground upset for reasons that could not be determined because postaccident examination of the helicopter revealed no evidence of mechanical malf…An on-ground upset for reasons that could not be determined because postaccident examination of the helicopter revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. |
| Jun 13, 2016 | Manchester, UK | G-BZGO | Incident | minor | Investigation pending |
| Jan 23, 2015 | Waikaia, NZ | ZK-HPC | Incident | substantial | Investigation pending |
| Mar 23, 2014 | Menard, TX | N44MD | Incident | substantial | The pilot’s inadequate recovery from a practice autorotation, which resulted in an improper touchdown attitude and collision with terrain. |
| Oct 18, 2013 | Sedro Woolley, WA | N414CC | Incident | substantial |
The non-instrument rated pilot's inadvertent encounter with instrument meteorological conditions during initial climb and his improper decision to con…The non-instrument rated pilot's inadvertent encounter with instrument meteorological conditions during initial climb and his improper decision to continue flight, which resulted in an in-flight impact with a tree and an emergency descent that resulted in a roll over on landing. |
| May 02, 2013 | Pomeroy, WA | N442RN | Incident | substantial |
The pilot's failure to ensure that the helicopter was properly loaded, which resulted in the helicopter being in excess of its maximum allowable gross…The pilot's failure to ensure that the helicopter was properly loaded, which resulted in the helicopter being in excess of its maximum allowable gross weight and led to a loss of main rotor rpm on takeoff. Contributing to the accident were the ground crewman's inadvertent overloading of the helicopter and the design of the spray tank's visual sight glass, which did not allow the pilot to visually verify the amount of the spray tank load without exiting the helicopter. |
| May 16, 2012 | Juuka, FI | OH-HZH | Incident | substantial | Investigation pending |
| Mar 31, 2011 | Straubing, GE | D-HBLT | Incident | destroyed | Investigation pending |
| Mar 17, 2011 | Petersburg, WV | N555FP | Incident | substantial | The pilot's failure to maintain control during the takeoff. |
| Feb 04, 2011 | Ogden, UT | N441TB | Incident | substantial |
The certified flight instructor’s failure to maintain adequate main rotor blade rpm during a practice autorotation, resulting in a hard landing and ro…The certified flight instructor’s failure to maintain adequate main rotor blade rpm during a practice autorotation, resulting in a hard landing and rollover. |
| Apr 06, 2010 | Temecula, CA | N688SS | Incident | substantial | The pilot's failure to maintain control of the helicopter during takeoff. |
| Oct 29, 2009 | San Juan Batista, CA | N144RF | Incident | substantial |
The pilot's failure to maintain adequate clearance from wires while maneuvering and his subsequent improper use of the collective control, which resul…The pilot's failure to maintain adequate clearance from wires while maneuvering and his subsequent improper use of the collective control, which resulted in the main rotor contacting the tail boom. |
| Sep 25, 2009 | Annerdale, SF | ZS-RMN | Incident | substantial | Investigation pending |
| Jul 19, 2009 | Silver Spring, PA | N25VH | Incident | substantial | The student pilot's inability to fully control the helicopter, during cruise and the resultant off-field hard landing. |
| May 03, 2009 | Cottonwood, AZ | N441CB | Incident | substantial | The pilot's inadequate visual lookout and failure to maintain clearance from wires. |
| Sep 06, 2008 | Marathon, FL | N144SA | Incident | substantial | The pilot's failure to control the helicopter while maneuvering, resulting in loss of tail rotor effectiveness. |
| Aug 23, 2008 | Iliamna, AK | N291VB | Incident | substantial |
The pilot's failure to see a wire cable prior to colliding with it. Factors contributing to the accident were the non-routine positioning of the wire …The pilot's failure to see a wire cable prior to colliding with it. Factors contributing to the accident were the non-routine positioning of the wire cable, and the ground crew's failure to advise the pilot that the wire had been re-routed. |
| Jul 04, 2008 | Ottawa, IL | N31138 | Incident | substantial | The pilot's failure to maintain clearance from the power transmission lines. Contributing to the accident was the unmarked power transmission lines. |