Mooney M20C Safety Record

Complete NTSB accident and incident history. 215 events recorded from 1982 to 2025.

215

All Events

91

Incidents

39

Minor

30

Serious

55

Fatal (95 fatalities)

Date Location Reg# Severity Damage Probable Cause
Jan 28, 2023 Calhoun, GA N5587Q Serious (1) destroyed A partial loss of engine power during the initial climb due to an improperly installed spark plug.
Apr 29, 2021 Warwick, NY N6448U Serious (1) substantial
A loose stand-off clamp which resulted in a throttle assembly malfunction, and the inability of the engine to produce full power during the attempted …

A loose stand-off clamp which resulted in a throttle assembly malfunction, and the inability of the engine to produce full power during the attempted takeoff.

Jun 02, 2020 Durham, NC N2768W Serious (1) substantial
The pilot’s failure to maintain proper airspeed and his exceedance of the airplane’s critical angle of attack, which resulted in an aerodynamic stall.…

The pilot’s failure to maintain proper airspeed and his exceedance of the airplane’s critical angle of attack, which resulted in an aerodynamic stall..

Aug 26, 2019 Reno, NV N78988 Serious (2) substantial The pilot's improper inflight fuel management, which resulted in fuel starvation and a total loss of engine power.
Nov 10, 2018 Wildwood, NJ N78870 Serious (1) substantial
The pilot’s improper fuel management, which resulted in a total loss of engine power due to fuel starvation during the initial climb. Contributing to …

The pilot’s improper fuel management, which resulted in a total loss of engine power due to fuel starvation during the initial climb. Contributing to the accident was the pilot’s decision to initiate a 180° turn following the loss of power.

Feb 03, 2017 Ellendale, MN N9149V Serious (1) substantial
The pilot’s incapacitation from carbon monoxide poisoning in flight due to cracks in the exhaust muffler, which resulted in the airplane’s continued f…

The pilot’s incapacitation from carbon monoxide poisoning in flight due to cracks in the exhaust muffler, which resulted in the airplane’s continued flight until it ran out of fuel and its subsequent collision with terrain.

Apr 18, 2015 Winchester, TN N9680M Serious (2) substantial
The pilot's inadequate weight and balance and performance planning, including his decision to take off with more passengers than permitted, and his ex…

The pilot's inadequate weight and balance and performance planning, including his decision to take off with more passengers than permitted, and his exceedance of the airplane’s critical angle of attack during the initial climb, which resulted in an aerodynamic stall and impact with terrain.

Nov 10, 2014 Lewisburg, WV N6581U Serious (1) substantial
The pilot's failure to maintain airspeed while maneuvering, which resulted in the airplane exceeding its critical angleofattack and experiencing an …

The pilot's failure to maintain airspeed while maneuvering, which resulted in the airplane exceeding its critical angleofattack and experiencing an aerodynamic stall. Contributing to the accident were abnormal engine operation due to improper magneto-to-engine ignition timing and the pilot's failure to have the airplane inspected before the flight as required by the special flight permit.

Aug 26, 2012 East Hampton, NY N557M Serious (2) substantial
A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any failures or malfunct…

A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any failures or malfunctions that would have precluded normal operation.

Nov 03, 2009 Fairview, NC N6896U Serious (2) substantial A total loss of engine power due to fuel exhaustion as a result of the pilot’s inadequate preflight fuel planning.
Dec 16, 2007 Phillipsburg, KS N63LH Serious (1) destroyed
Total loss of engine power due to contamination of the carburetor, total blockage of the fuel inlet screen, and partial blockage of the fuel lines and…

Total loss of engine power due to contamination of the carburetor, total blockage of the fuel inlet screen, and partial blockage of the fuel lines and fittings. Contributing to the accident were the dark night light conditions and the trees.

Jun 10, 2004 Golden, MO N3911N Serious (1) substantial The pilot's failure to maintain directional control and his failure to maintain clearance from the trees. The trees were a contributing factor.
Aug 31, 2003 Watsonville, CA N707JH Serious (3) substantial
the non-instrument rated pilot's intentional continuance of VFR flight into instrument meteorological conditions and failure to maintain clearance wit…

the non-instrument rated pilot's intentional continuance of VFR flight into instrument meteorological conditions and failure to maintain clearance with terrain.

Apr 01, 2003 Lakeland, FL N2652W Serious minor
The inadequate visual lookout of the pilot and the ground marshaller resulting in the ground marshaller being struck by the wing of the taxiing airpla…

The inadequate visual lookout of the pilot and the ground marshaller resulting in the ground marshaller being struck by the wing of the taxiing airplane and receiving serious injury.

Jan 13, 2001 Somerset, MA N1398W Serious (1) substantial The pilot's inadequate visual lookout. A factor was the dusk lighting conditions.
Nov 28, 1999 HILLSBORO, TX N6766U Serious (1) substantial The pilot's failure to maintain directional control of the airplane during the go-around. A factor was the gust of wind.
Oct 21, 1998 ENGLEWOOD, CO N6405U Serious (1) substantial
The undertorquing of the camshaft gear retaining bolts during engine overhaul by maintenance personnel. A factor was the unsuitable terrain for a for…

The undertorquing of the camshaft gear retaining bolts during engine overhaul by maintenance personnel. A factor was the unsuitable terrain for a forced landing.

Aug 10, 1997 BOUNTIFUL, UT N9666M Serious (1) substantial The pilot's inadequate fuel management which resulted in fuel starvation.
Jul 05, 1994 LAS VEGAS, NV N6959U Serious (1) substantial THE FAILURE OF THE PILOT TO OBTAIN THE PROPER TAKEOFF SPEED. FACTORS ARE THE HIGH DENSITY ALTITUDE AND THE CROSSWIND.
Sep 19, 1993 CRIVITZ, WI N6752N Serious (1) substantial fuel starvation caused by foreign matter in the fuel tank strainer.
Mar 10, 1991 LOA, UT N7108U Serious (1) substantial
THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN AIRSPEED ON TAKEOFF CLIMB IN A TURN RESULTING IN AN INADVERTNENT STALL AND SUBSEQUENT IN FLIGHT COLLISION W…

THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN AIRSPEED ON TAKEOFF CLIMB IN A TURN RESULTING IN AN INADVERTNENT STALL AND SUBSEQUENT IN FLIGHT COLLISION WITH TERRAIN. CONTRIBUTING TO THE ACCIDENT WAS A CROSSWIND WITH GUSTS.

Oct 07, 1990 KISSIMMEE, FL N1389W Serious (2) substantial
MALFUNCTION OF BOTH MAGNETOS DUE TO DETERIORATION OF THE COILS, FAILURE OF MAINTENANCE PERSONNEL TO COMPLY WITH AN AIRWORTHINESS DIRECTIVE, AND FAILUR…

MALFUNCTION OF BOTH MAGNETOS DUE TO DETERIORATION OF THE COILS, FAILURE OF MAINTENANCE PERSONNEL TO COMPLY WITH AN AIRWORTHINESS DIRECTIVE, AND FAILURE OF THE PILOT TO MAINTAIN ADEQUATE VISUAL LOOKOUT WHILE ON AN APPROACH FOR AN EMERGENCY LANDING. FACTORS RELATED TO THE ACCIDENT WERE: THE OBSTRUCTION (TREE) IN THE EMERGENCY LANDING AREA, AND DIVERSION OF THE PILOT'S ATTENTION WHILE APPROACHING TO LAND.

Jun 18, 1990 TROUTDALE, OR N8165E Serious (2) substantial AN INADEQUATE ANNUAL INSPECTION IN WHICH MAINTENANCE PERSONNEL LEFT AN OBJECT IN THE AREA OF THE CARBURETOR WHICH RESULTED IN AN AIR FLOW BLOCKAGE.
Apr 28, 1990 LITTLE ROCK, AR N6824N Serious (1) substantial
PILOT IN COMMAND'S FAILURE TO REFUEL THE AIRPLANE, WHICH RESULTED IN FUEL EXHAUSTION. RELATED TO THE ACCIDENT WAS: UNSUITABLE TERRAIN IN THE EMERGENC…

PILOT IN COMMAND'S FAILURE TO REFUEL THE AIRPLANE, WHICH RESULTED IN FUEL EXHAUSTION. RELATED TO THE ACCIDENT WAS: UNSUITABLE TERRAIN IN THE EMERGENCY LANDING AREA.

Sep 18, 1989 NEIHART, MT N3456X Serious (1) destroyed
VFR FLIGHT BY THE PILOT INTO INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) AND HIS FAILURE TO MAINTAIN SUFFICIENT ALTITUDE. RELATED FACTORS WERE: THE H…

VFR FLIGHT BY THE PILOT INTO INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) AND HIS FAILURE TO MAINTAIN SUFFICIENT ALTITUDE. RELATED FACTORS WERE: THE HIGH TERRAIN AND ADVERSE WEATHER CONDITIONS.

Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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