Mooney M20C Safety Record
Complete NTSB accident and incident history. 215 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jan 28, 2023 | Calhoun, GA | N5587Q | Serious (1) | destroyed | A partial loss of engine power during the initial climb due to an improperly installed spark plug. |
| Apr 29, 2021 | Warwick, NY | N6448U | Serious (1) | substantial |
A loose stand-off clamp which resulted in a throttle assembly malfunction, and the inability of the engine to produce full power during the attempted …A loose stand-off clamp which resulted in a throttle assembly malfunction, and the inability of the engine to produce full power during the attempted takeoff. |
| Jun 02, 2020 | Durham, NC | N2768W | Serious (1) | substantial |
The pilot’s failure to maintain proper airspeed and his exceedance of the airplane’s critical angle of attack, which resulted in an aerodynamic stall.…The pilot’s failure to maintain proper airspeed and his exceedance of the airplane’s critical angle of attack, which resulted in an aerodynamic stall.. |
| Aug 26, 2019 | Reno, NV | N78988 | Serious (2) | substantial | The pilot's improper inflight fuel management, which resulted in fuel starvation and a total loss of engine power. |
| Nov 10, 2018 | Wildwood, NJ | N78870 | Serious (1) | substantial |
The pilot’s improper fuel management, which resulted in a total loss of engine power due to fuel starvation during the initial climb. Contributing to …The pilot’s improper fuel management, which resulted in a total loss of engine power due to fuel starvation during the initial climb. Contributing to the accident was the pilot’s decision to initiate a 180° turn following the loss of power. |
| Feb 03, 2017 | Ellendale, MN | N9149V | Serious (1) | substantial |
The pilot’s incapacitation from carbon monoxide poisoning in flight due to cracks in the exhaust muffler, which resulted in the airplane’s continued f…The pilot’s incapacitation from carbon monoxide poisoning in flight due to cracks in the exhaust muffler, which resulted in the airplane’s continued flight until it ran out of fuel and its subsequent collision with terrain. |
| Apr 18, 2015 | Winchester, TN | N9680M | Serious (2) | substantial |
The pilot's inadequate weight and balance and performance planning, including his decision to take off with more passengers than permitted, and his ex…The pilot's inadequate weight and balance and performance planning, including his decision to take off with more passengers than permitted, and his exceedance of the airplane’s critical angle of attack during the initial climb, which resulted in an aerodynamic stall and impact with terrain. |
| Nov 10, 2014 | Lewisburg, WV | N6581U | Serious (1) | substantial |
The pilot's failure to maintain airspeed while maneuvering, which resulted in the airplane exceeding its critical angleofattack and experiencing an …The pilot's failure to maintain airspeed while maneuvering, which resulted in the airplane exceeding its critical angleofattack and experiencing an aerodynamic stall. Contributing to the accident were abnormal engine operation due to improper magneto-to-engine ignition timing and the pilot's failure to have the airplane inspected before the flight as required by the special flight permit. |
| Aug 26, 2012 | East Hampton, NY | N557M | Serious (2) | substantial |
A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any failures or malfunct…A loss of engine power for reasons that could not be determined because postaccident examination of the engine did not reveal any failures or malfunctions that would have precluded normal operation. |
| Nov 03, 2009 | Fairview, NC | N6896U | Serious (2) | substantial | A total loss of engine power due to fuel exhaustion as a result of the pilot’s inadequate preflight fuel planning. |
| Dec 16, 2007 | Phillipsburg, KS | N63LH | Serious (1) | destroyed |
Total loss of engine power due to contamination of the carburetor, total blockage of the fuel inlet screen, and partial blockage of the fuel lines and…Total loss of engine power due to contamination of the carburetor, total blockage of the fuel inlet screen, and partial blockage of the fuel lines and fittings. Contributing to the accident were the dark night light conditions and the trees. |
| Jun 10, 2004 | Golden, MO | N3911N | Serious (1) | substantial | The pilot's failure to maintain directional control and his failure to maintain clearance from the trees. The trees were a contributing factor. |
| Aug 31, 2003 | Watsonville, CA | N707JH | Serious (3) | substantial |
the non-instrument rated pilot's intentional continuance of VFR flight into instrument meteorological conditions and failure to maintain clearance wit…the non-instrument rated pilot's intentional continuance of VFR flight into instrument meteorological conditions and failure to maintain clearance with terrain. |
| Apr 01, 2003 | Lakeland, FL | N2652W | Serious | minor |
The inadequate visual lookout of the pilot and the ground marshaller resulting in the ground marshaller being struck by the wing of the taxiing airpla…The inadequate visual lookout of the pilot and the ground marshaller resulting in the ground marshaller being struck by the wing of the taxiing airplane and receiving serious injury. |
| Jan 13, 2001 | Somerset, MA | N1398W | Serious (1) | substantial | The pilot's inadequate visual lookout. A factor was the dusk lighting conditions. |
| Nov 28, 1999 | HILLSBORO, TX | N6766U | Serious (1) | substantial | The pilot's failure to maintain directional control of the airplane during the go-around. A factor was the gust of wind. |
| Oct 21, 1998 | ENGLEWOOD, CO | N6405U | Serious (1) | substantial |
The undertorquing of the camshaft gear retaining bolts during engine overhaul by maintenance personnel. A factor was the unsuitable terrain for a for…The undertorquing of the camshaft gear retaining bolts during engine overhaul by maintenance personnel. A factor was the unsuitable terrain for a forced landing. |
| Aug 10, 1997 | BOUNTIFUL, UT | N9666M | Serious (1) | substantial | The pilot's inadequate fuel management which resulted in fuel starvation. |
| Jul 05, 1994 | LAS VEGAS, NV | N6959U | Serious (1) | substantial | THE FAILURE OF THE PILOT TO OBTAIN THE PROPER TAKEOFF SPEED. FACTORS ARE THE HIGH DENSITY ALTITUDE AND THE CROSSWIND. |
| Sep 19, 1993 | CRIVITZ, WI | N6752N | Serious (1) | substantial | fuel starvation caused by foreign matter in the fuel tank strainer. |
| Mar 10, 1991 | LOA, UT | N7108U | Serious (1) | substantial |
THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN AIRSPEED ON TAKEOFF CLIMB IN A TURN RESULTING IN AN INADVERTNENT STALL AND SUBSEQUENT IN FLIGHT COLLISION W…THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN AIRSPEED ON TAKEOFF CLIMB IN A TURN RESULTING IN AN INADVERTNENT STALL AND SUBSEQUENT IN FLIGHT COLLISION WITH TERRAIN. CONTRIBUTING TO THE ACCIDENT WAS A CROSSWIND WITH GUSTS. |
| Oct 07, 1990 | KISSIMMEE, FL | N1389W | Serious (2) | substantial |
MALFUNCTION OF BOTH MAGNETOS DUE TO DETERIORATION OF THE COILS, FAILURE OF MAINTENANCE PERSONNEL TO COMPLY WITH AN AIRWORTHINESS DIRECTIVE, AND FAILUR…MALFUNCTION OF BOTH MAGNETOS DUE TO DETERIORATION OF THE COILS, FAILURE OF MAINTENANCE PERSONNEL TO COMPLY WITH AN AIRWORTHINESS DIRECTIVE, AND FAILURE OF THE PILOT TO MAINTAIN ADEQUATE VISUAL LOOKOUT WHILE ON AN APPROACH FOR AN EMERGENCY LANDING. FACTORS RELATED TO THE ACCIDENT WERE: THE OBSTRUCTION (TREE) IN THE EMERGENCY LANDING AREA, AND DIVERSION OF THE PILOT'S ATTENTION WHILE APPROACHING TO LAND. |
| Jun 18, 1990 | TROUTDALE, OR | N8165E | Serious (2) | substantial | AN INADEQUATE ANNUAL INSPECTION IN WHICH MAINTENANCE PERSONNEL LEFT AN OBJECT IN THE AREA OF THE CARBURETOR WHICH RESULTED IN AN AIR FLOW BLOCKAGE. |
| Apr 28, 1990 | LITTLE ROCK, AR | N6824N | Serious (1) | substantial |
PILOT IN COMMAND'S FAILURE TO REFUEL THE AIRPLANE, WHICH RESULTED IN FUEL EXHAUSTION. RELATED TO THE ACCIDENT WAS: UNSUITABLE TERRAIN IN THE EMERGENC…PILOT IN COMMAND'S FAILURE TO REFUEL THE AIRPLANE, WHICH RESULTED IN FUEL EXHAUSTION. RELATED TO THE ACCIDENT WAS: UNSUITABLE TERRAIN IN THE EMERGENCY LANDING AREA. |
| Sep 18, 1989 | NEIHART, MT | N3456X | Serious (1) | destroyed |
VFR FLIGHT BY THE PILOT INTO INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) AND HIS FAILURE TO MAINTAIN SUFFICIENT ALTITUDE. RELATED FACTORS WERE: THE H…VFR FLIGHT BY THE PILOT INTO INSTRUMENT METEOROLOGICAL CONDITIONS (IMC) AND HIS FAILURE TO MAINTAIN SUFFICIENT ALTITUDE. RELATED FACTORS WERE: THE HIGH TERRAIN AND ADVERSE WEATHER CONDITIONS. |