Mooney M20C Safety Record
Complete NTSB accident and incident history. 215 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jan 01, 2022 | Southeast Arcadia, FL | N79396 | Minor | substantial | The total loss of engine power for reasons that could not be determined based on the available evidence for this investigation. |
| Nov 09, 2020 | Laconia, NH | N3296F | Minor | substantial | The pilot’s failure to maintain adequate clearance from trees during an approach in sun glare and hazy conditions. |
| Apr 21, 2016 | Sand Springs, OK | N6870N | Minor | substantial | A total loss of engine power due to fuel starvation. Contributing to the accident was the pilot's inadequate preflight inspection. |
| Mar 18, 2016 | Wichita, KS | N9262M | Minor | substantial | The total loss of engine power due to fuel starvation, which resulted from the pilot's improper fuel management. |
| May 19, 2012 | Pembroke Pines, FL | N2610W | Minor | substantial | The pilot's improper fuel management, which resulted in a total loss of engine power during approach due to fuel exhaustion. |
| Sep 11, 2011 | Kokomo, IN | N9266M | Minor | substantial |
The loss of engine power following takeoff for reasons that could not be determined because postaccident examination did not reveal any anomalies that…The loss of engine power following takeoff for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation. |
| Aug 30, 2011 | Allen, OK | N5501Q | Minor | substantial | A total loss of engine power in flight due to fuel starvation as a result of the pilot’s inadequate fuel management. |
| Oct 10, 2009 | Marathon, FL | N2558Y | Minor | destroyed | A total loss of engine power for undetermined reasons. |
| Sep 17, 2008 | Bolingbrook, IL | N5651Q | Minor | substantial |
The non-mechanical loss of engine power due to the pilot's incorrect positioning of the fuel tank selector prior to takeoff and the subsequent fuel st…The non-mechanical loss of engine power due to the pilot's incorrect positioning of the fuel tank selector prior to takeoff and the subsequent fuel starvation during takeoff. |
| Sep 09, 2008 | Wallace, NC | N21MY | Minor | substantial |
The pilot's failure to abort the takeoff when the engine failed to develop full power. Contributing to the accident was the pilot's failure to remove …The pilot's failure to abort the takeoff when the engine failed to develop full power. Contributing to the accident was the pilot's failure to remove the intake plugs prior to takeoff. |
| Apr 16, 2007 | Sidney, OH | N3529H | Minor | substantial |
The total loss of engine power during initial climb due to oil starvation as a result of improper maintenance. The fixed base operator's failure to ad…The total loss of engine power during initial climb due to oil starvation as a result of improper maintenance. The fixed base operator's failure to advise the pilot that the engine had been operated without oil in the engine and soft terrain were factors. |
| Sep 20, 2006 | Auburn, CA | N5577Q | Minor | substantial |
the fatigue failure of the elevator's control rod due to inadequate lubrication. Contributing factors were the inadequate maintenance and the owner-p…the fatigue failure of the elevator's control rod due to inadequate lubrication. Contributing factors were the inadequate maintenance and the owner-pilot's failure to comply with an airworthiness directive. |
| Jul 09, 2006 | El Dorado, TX | N6697U | Minor | substantial |
The pilot's failure to switch fuel tanks during cruise flight, which resulted in a loss of engine power due to fuel starvation. A contributing factor…The pilot's failure to switch fuel tanks during cruise flight, which resulted in a loss of engine power due to fuel starvation. A contributing factor was the lack of suitable terrain for the forced landing. |
| Feb 23, 2006 | Cottage Grove, OR | N6595U | Minor | substantial |
Fuel starvation while on approach for landing resulting in a loss of engine power, and an inadequately accomplished annual inspection. Incorrect hard…Fuel starvation while on approach for landing resulting in a loss of engine power, and an inadequately accomplished annual inspection. Incorrect hardware which impeded the movement of the fuel selector valve, improper fuel management and not identifying the proper fuel selector position were factors. |
| Jul 13, 2003 | Utica, OH | N33WL | Minor | substantial | The pilot's improper fuel consumption calculations, which resulted in fuel exhaustion. A factor was the unsuitable terrain. |
| Mar 09, 2003 | Colo Springs, CO | N9313V | Minor | substantial |
the pilot's failure to maintain aircraft control during initial climb which resulted in impact with terrain. Contributing factors include the downdra…the pilot's failure to maintain aircraft control during initial climb which resulted in impact with terrain. Contributing factors include the downdraft, crosswind and gusty wind conditions. |
| Dec 30, 2001 | Martinsville, VA | N6779U | Minor | substantial | The pilot's premature rotation and his failure to maintain directional control during the takeoff roll. |
| Aug 07, 2001 | Fort Lauderdale, FL | N78933 | Minor | substantial |
The failure of the mechanic who installed the carburetor after overhaul to safety the throttle linkage at the carburetor per an Airworthiness Directiv…The failure of the mechanic who installed the carburetor after overhaul to safety the throttle linkage at the carburetor per an Airworthiness Directive resulting in separation of the throttle linkage and subsequent partial loss of engine power. Contributing to the accident was the unsuitable terrain encountered by the pilot-in-command during the forced landing. |
| Nov 30, 2000 | HAZARD, KY | N942TB | Minor | — |
The incorrect routing of the cabin air scat tubing by an unknown person, which resulted in a carbon monoxide leak into the cabin, and subsequent pilot…The incorrect routing of the cabin air scat tubing by an unknown person, which resulted in a carbon monoxide leak into the cabin, and subsequent pilot incapacitation. |
| Jun 29, 2000 | WHITNEY, TX | N6932N | Minor | substantial | The partial loss of engine power, which resulted from the worn carburetor. |
| Apr 20, 2000 | MIDDLETOWN, RI | N9187V | Minor | substantial | an inadequate preflight inspection by the pilot which did not detect the water in the fuel tanks prior to departure. |
| Mar 22, 1999 | IRVING, NY | N5878Q | Minor | substantial | was the pilot's intentional flight into known icing conditions. |
| Jun 24, 1997 | BELLWOOD, PA | N6756N | Minor | substantial | the total loss of engine power due to failed connecting rods. |
| May 09, 1997 | TORREON, NM | N7853V | Minor | substantial |
failure of the forward number four piston pin plug, and the subsequent obstruction of internal oil passages of the lubricating system, which resulted …failure of the forward number four piston pin plug, and the subsequent obstruction of internal oil passages of the lubricating system, which resulted in partial loss of engine power. Factors relating to the accident were: the crosswind condition and lack of suitable terrain for an emergency (precautionary) landing. |
| Mar 17, 1996 | KINGSTON, TN | N78896 | Minor | substantial |
The pilot's inadequate pre-flight inspection, which resulted in fuel exhaustion. A factor relating to the accident was: the lack of suitable terrain …The pilot's inadequate pre-flight inspection, which resulted in fuel exhaustion. A factor relating to the accident was: the lack of suitable terrain for the forced landing. |