Mooney M20 Safety Record
Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 09, 2017 | Myrtle Beach, SC | N20835 | Incident | substantial |
A total loss of engine power during initial climb for reasons that could not be determined because the airplane sank in the ocean and was not recovere…A total loss of engine power during initial climb for reasons that could not be determined because the airplane sank in the ocean and was not recovered. |
| Apr 28, 2017 | Cedar Key, FL | N1157N | Incident | substantial | The pilot’s failure to follow the manufacturer’s go-around procedure, which resulted in an aerodynamic stall. |
| Mar 04, 2017 | Hebron, NE | N381LB | Incident | substantial | A loss of directional control during landing for reasons that could be determined based on the available information. |
| Oct 23, 2016 | Coalinga, CA | N201EU | Incident | substantial | A partial loss of engine power due to the pilot's improper in-flight fuel management, which resulted in fuel starvation. |
| Jun 18, 2016 | Clifton, TN | N3877H | Incident | substantial | The flight's encounter with unforecast extreme turbulence, which resulted in a loss of airplane control and structural damage. |
| Jun 04, 2016 | Williamstown, NJ | N6453U | Incident | substantial |
The pilot's landing area overshoot and failure to maintain surface speed and braking capability, which resulted in a runway overrun and a collision wi…The pilot's landing area overshoot and failure to maintain surface speed and braking capability, which resulted in a runway overrun and a collision with a fence. |
| May 13, 2016 | Little Rock, AR | N6371Q | Incident | substantial | A loss of engine power due to water contamination of the fuel. |
| Feb 22, 2016 | Pacoima, CA | N201KY | Incident | substantial |
A total loss of engine power for reasons that could not be determined because postaccident examination did not reveal any evidence of preimpact mechan…A total loss of engine power for reasons that could not be determined because postaccident examination did not reveal any evidence of preimpact mechanical failures or malfunctions that would have precluded normal operation. |
| Dec 14, 2015 | Corona, CA | N5863Q | Incident | substantial |
A partial loss of engine power during initial climb for reasons that could not be determined based on available information. Contributing to the accid…A partial loss of engine power during initial climb for reasons that could not be determined based on available information. Contributing to the accident was the pilot’s decision to conduct the takeoff with observed engine deficiencies. |
| Nov 27, 2015 | Farmington, DE | N201HK | Incident | substantial |
Both pilots' failure to maintain visual separation during landing at an uncontrolled airport. Contributing to the accident was the Mooney pilot's lack…Both pilots' failure to maintain visual separation during landing at an uncontrolled airport. Contributing to the accident was the Mooney pilot's lack of prompt evasive action once the biplane had been spotted on the same runway. In addition, the biplane pilots failure to ensure a clear runway. |
| Nov 22, 2015 | Fort Meade, MD | N5512Q | Incident | substantial |
A partial loss of engine power for reasons that could not be determined because postaccident examination of the engine revealed no mechanical malfunct…A partial loss of engine power for reasons that could not be determined because postaccident examination of the engine revealed no mechanical malfunctions or failures that would have precluded normal operation. |
| Sep 19, 2015 | Manville, NJ | N763RC | Incident | substantial | The pilot's failure to maintain directional control during the takeoff roll, which resulted in a runway excursion and collision with a fence. |
| Jun 27, 2015 | West Mifflin, PA | N93TK | Incident | substantial |
The pilot's failure to maintain pitch control during landing, which resulted in a bounce and loss of control during landing, followed by a runway excu…The pilot's failure to maintain pitch control during landing, which resulted in a bounce and loss of control during landing, followed by a runway excursion, and collision with terrain during an attempt to abort the landing. |
| Jun 21, 2015 | Sheboygan, WI | N1168Z | Incident | substantial |
Oil starvation due to preignition in the No. 5 cylinder as a result of failed spark plugs; the top and sides of the piston head were eroded, which all…Oil starvation due to preignition in the No. 5 cylinder as a result of failed spark plugs; the top and sides of the piston head were eroded, which allowed the exhaust gases caused by the preignition to pressurize the crankcase and force engine oil out of the breather tube. |
| Jun 08, 2015 | Reno, NV | N7887V | Incident | destroyed | The in-flight separation of the exhaust tube at a weld joint due to erosion and corrosion, which resulted in a subsequent in-flight fire. |
| Apr 06, 2015 | Allentown, PA | N4826H | Incident | substantial |
A total loss of engine power during takeoff due to an interruption of fuel flow to the engine. The reason for the interruption of the fuel flow could …A total loss of engine power during takeoff due to an interruption of fuel flow to the engine. The reason for the interruption of the fuel flow could not be determined during postaccident examination and testing. |
| Feb 14, 2015 | Bakersfield, CA | N11LV | Incident | substantial |
The collapse of all three landing gear during the takeoff roll for reasons that could not be determined because postaccident examination did not revea…The collapse of all three landing gear during the takeoff roll for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation. |
| Jan 17, 2015 | Lonoke county, AR | N6474U | Incident | substantial | The loss of engine power due to fuel starvation. |
| May 11, 2014 | Dowling, MI | N343ED | Incident | substantial | The pilot's failure to maintain control during landing. |
| Jan 26, 2014 | Rutherfordton, NC | N6762U | Incident | substantial |
The pilot's inadequate pre-flight planning and in-flight monitoring of the fuel level which resulted in a total loss of engine power due to fuel exhau…The pilot's inadequate pre-flight planning and in-flight monitoring of the fuel level which resulted in a total loss of engine power due to fuel exhaustion. |
| Nov 07, 2013 | Fort Collins, CO | N1006A | Incident | substantial | The pilot did not maintain control of the airplane during the go around. |
| Sep 15, 2013 | Lund, NV | N1079K | Incident | substantial |
The pilot’s failure to monitor the environment, which led to a collision with power lines during climbout. Contributing to the accident was the loss o…The pilot’s failure to monitor the environment, which led to a collision with power lines during climbout. Contributing to the accident was the loss of engine power during low-altitude flight for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any mechanical malfunctions or failures that would have precluded normal operation, which led to a forced landing that the pilot subsequently aborted when the engine regained full power. |
| Aug 04, 2013 | Tallahassee, FL | N1034S | Incident | substantial |
The pilot's failure to troubleshoot the in-flight electrical problem and restore power using the operable redundant battery and his decision not to ma…The pilot's failure to troubleshoot the in-flight electrical problem and restore power using the operable redundant battery and his decision not to manually extend the airplane's landing gear, which resulted in a gear-up landing. Contributing to the accident was an internal electrical short of the No. 2 battery, which resulted in a total loss of electrical power. |
| Aug 02, 2013 | Helena, MT | N2926M | Incident | substantial | The flight instructor's delayed decision to instruct the pilot to abort the landing which resulted in a runway excursion and collision with a fence. |
| Jun 25, 2013 | El Reno, OK | N205MC | Incident | substantial |
A loss of engine power, which resulted from the failure of the magneto assembly for reasons that could not be determined during postaccident examinati…A loss of engine power, which resulted from the failure of the magneto assembly for reasons that could not be determined during postaccident examinations. |