Mooney M20 Safety Record

Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.

1232

All Events

546

Incidents

193

Minor

137

Serious

353

Fatal (633 fatalities)

Date Location Reg# Severity Damage Probable Cause
Feb 03, 2003 New Orleans, LA N658FT Minor substantial
The loss of engine power as a result of the separation of the magneto assembly due to inadequate maintenance by unknown personnel. A contributing fac…

The loss of engine power as a result of the separation of the magneto assembly due to inadequate maintenance by unknown personnel. A contributing factor was the lack of suitable terrain for the forced landing.

Jan 28, 2003 Myrtle Beach, SC N231NT Minor substantial A loss of engine power for undetermined reasons.
Sep 07, 2002 Rector, AR N6369Q Minor substantial The pilot's failure to maintain adequate airspeed which resulted in an inadvertent stall.
Aug 08, 2002 Gualala, CA N1038K Minor destroyed
The pilot's delayed decision in executing a go-around. Contributing factors were the pilot's limited experience landing on short fields and the risin…

The pilot's delayed decision in executing a go-around. Contributing factors were the pilot's limited experience landing on short fields and the rising terrain.

May 23, 2002 Charleston, SC N4560H Minor substantial Total loss of engine power due to oil system starvation. A factor was the transmission wire encountered during emergency descent.
Mar 16, 2002 Norman, OK N8390E Minor substantial Maintenance personnel's improper clamp installation on the mixture control cable, which resulted in a loss of engine power.
Jan 19, 2002 Glasgow, MT N38AJ Minor substantial
The pilot's failure to maintain adequate flying airspeed resulting in a stall/mush condition and loss of control at low altitude. A contributing fact…

The pilot's failure to maintain adequate flying airspeed resulting in a stall/mush condition and loss of control at low altitude. A contributing factor was the pilot's distraction from flying the aircraft while attempting to retract the landing gear.

Jan 17, 2002 Lake Placid, FL N201XL Minor destroyed
The failure of the pilot to perform a proper preflight inspection and his improper fuel tank selection for takeoff, resulting in a loss of engine powe…

The failure of the pilot to perform a proper preflight inspection and his improper fuel tank selection for takeoff, resulting in a loss of engine power on takeoff due to fuel starvation, and the pilot's failure to maintain directional control of the aircraft resulting in an uncontrollable descent and collision with orange trees and terrain.

Dec 30, 2001 Martinsville, VA N6779U Minor substantial The pilot's premature rotation and his failure to maintain directional control during the takeoff roll.
Aug 07, 2001 Fort Lauderdale, FL N78933 Minor substantial
The failure of the mechanic who installed the carburetor after overhaul to safety the throttle linkage at the carburetor per an Airworthiness Directiv…

The failure of the mechanic who installed the carburetor after overhaul to safety the throttle linkage at the carburetor per an Airworthiness Directive resulting in separation of the throttle linkage and subsequent partial loss of engine power. Contributing to the accident was the unsuitable terrain encountered by the pilot-in-command during the forced landing.

Dec 05, 2000 DANBURY, CT N4101H Minor substantial Water/ice in the fuel system and the pilot's inadequate preflight inspection.
Nov 30, 2000 HAZARD, KY N942TB Minor
The incorrect routing of the cabin air scat tubing by an unknown person, which resulted in a carbon monoxide leak into the cabin, and subsequent pilot…

The incorrect routing of the cabin air scat tubing by an unknown person, which resulted in a carbon monoxide leak into the cabin, and subsequent pilot incapacitation.

Nov 13, 2000 LONGMONT, CO N201JP Minor substantial
the total failure of the left main gear strut during the landing roll. A contributing factor was the 6-foot high snow bank that the airplane impacted…

the total failure of the left main gear strut during the landing roll. A contributing factor was the 6-foot high snow bank that the airplane impacted when it left the runway.

Sep 28, 2000 SAN CARLOS, CA N68FM Minor substantial The pilot's failure to maintain directional control of the airplane during an aborted landing.
Aug 02, 2000 OREGON CITY, OR N1927Y Minor substantial A loss of engine power for undetermined reason(s). A factor was the rough/uneven terrain.
Jul 01, 2000 GODLEY, TX N231RR Minor substantial The pilot's inadequate preflight planning and his delay in aborting the takeoff.
Jun 29, 2000 WHITNEY, TX N6932N Minor substantial The partial loss of engine power, which resulted from the worn carburetor.
Jun 03, 2000 UPLAND, CA N9207V Minor substantial The failure of the pilot-in-command to maintain directional control of the aircraft on takeoff after the cabin door became ajar.
Apr 20, 2000 MIDDLETOWN, RI N9187V Minor substantial an inadequate preflight inspection by the pilot which did not detect the water in the fuel tanks prior to departure.
Apr 19, 2000 TOMBALL, TX N7038V Minor substantial Engine seizure due to the rupture of an oil cooler line.
Dec 11, 1999 READING, PA N6715U Minor substantial The failure of the number two connecting rod after an improper overhaul by maintenance personnel.
Aug 28, 1999 EMIGRANT GAP, CA N4201S Minor substantial
The fatigue failure and separation of the number three cylinder due to the cylinder overhaul facility's improper inspection and quality control proces…

The fatigue failure and separation of the number three cylinder due to the cylinder overhaul facility's improper inspection and quality control processes.

Jul 19, 1999 MARSHALL, MN N7141V Minor substantial
the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landi…

the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landing attempt by the pilot.

Jun 16, 1999 CANON CITY, CO N9355M Minor destroyed
The pilot's poor judgement due to his intentional and continued flight into instrument meteorological conditions. Factors were the existing weather co…

The pilot's poor judgement due to his intentional and continued flight into instrument meteorological conditions. Factors were the existing weather conditions that included clouds and obscuration.

Mar 22, 1999 IRVING, NY N5878Q Minor substantial was the pilot's intentional flight into known icing conditions.
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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Data source: NTSB Aviation Accident Database · About our data