Mooney M20 Safety Record
Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Feb 03, 2003 | New Orleans, LA | N658FT | Minor | substantial |
The loss of engine power as a result of the separation of the magneto assembly due to inadequate maintenance by unknown personnel. A contributing fac…The loss of engine power as a result of the separation of the magneto assembly due to inadequate maintenance by unknown personnel. A contributing factor was the lack of suitable terrain for the forced landing. |
| Jan 28, 2003 | Myrtle Beach, SC | N231NT | Minor | substantial | A loss of engine power for undetermined reasons. |
| Sep 07, 2002 | Rector, AR | N6369Q | Minor | substantial | The pilot's failure to maintain adequate airspeed which resulted in an inadvertent stall. |
| Aug 08, 2002 | Gualala, CA | N1038K | Minor | destroyed |
The pilot's delayed decision in executing a go-around. Contributing factors were the pilot's limited experience landing on short fields and the risin…The pilot's delayed decision in executing a go-around. Contributing factors were the pilot's limited experience landing on short fields and the rising terrain. |
| May 23, 2002 | Charleston, SC | N4560H | Minor | substantial | Total loss of engine power due to oil system starvation. A factor was the transmission wire encountered during emergency descent. |
| Mar 16, 2002 | Norman, OK | N8390E | Minor | substantial | Maintenance personnel's improper clamp installation on the mixture control cable, which resulted in a loss of engine power. |
| Jan 19, 2002 | Glasgow, MT | N38AJ | Minor | substantial |
The pilot's failure to maintain adequate flying airspeed resulting in a stall/mush condition and loss of control at low altitude. A contributing fact…The pilot's failure to maintain adequate flying airspeed resulting in a stall/mush condition and loss of control at low altitude. A contributing factor was the pilot's distraction from flying the aircraft while attempting to retract the landing gear. |
| Jan 17, 2002 | Lake Placid, FL | N201XL | Minor | destroyed |
The failure of the pilot to perform a proper preflight inspection and his improper fuel tank selection for takeoff, resulting in a loss of engine powe…The failure of the pilot to perform a proper preflight inspection and his improper fuel tank selection for takeoff, resulting in a loss of engine power on takeoff due to fuel starvation, and the pilot's failure to maintain directional control of the aircraft resulting in an uncontrollable descent and collision with orange trees and terrain. |
| Dec 30, 2001 | Martinsville, VA | N6779U | Minor | substantial | The pilot's premature rotation and his failure to maintain directional control during the takeoff roll. |
| Aug 07, 2001 | Fort Lauderdale, FL | N78933 | Minor | substantial |
The failure of the mechanic who installed the carburetor after overhaul to safety the throttle linkage at the carburetor per an Airworthiness Directiv…The failure of the mechanic who installed the carburetor after overhaul to safety the throttle linkage at the carburetor per an Airworthiness Directive resulting in separation of the throttle linkage and subsequent partial loss of engine power. Contributing to the accident was the unsuitable terrain encountered by the pilot-in-command during the forced landing. |
| Dec 05, 2000 | DANBURY, CT | N4101H | Minor | substantial | Water/ice in the fuel system and the pilot's inadequate preflight inspection. |
| Nov 30, 2000 | HAZARD, KY | N942TB | Minor | — |
The incorrect routing of the cabin air scat tubing by an unknown person, which resulted in a carbon monoxide leak into the cabin, and subsequent pilot…The incorrect routing of the cabin air scat tubing by an unknown person, which resulted in a carbon monoxide leak into the cabin, and subsequent pilot incapacitation. |
| Nov 13, 2000 | LONGMONT, CO | N201JP | Minor | substantial |
the total failure of the left main gear strut during the landing roll. A contributing factor was the 6-foot high snow bank that the airplane impacted…the total failure of the left main gear strut during the landing roll. A contributing factor was the 6-foot high snow bank that the airplane impacted when it left the runway. |
| Sep 28, 2000 | SAN CARLOS, CA | N68FM | Minor | substantial | The pilot's failure to maintain directional control of the airplane during an aborted landing. |
| Aug 02, 2000 | OREGON CITY, OR | N1927Y | Minor | substantial | A loss of engine power for undetermined reason(s). A factor was the rough/uneven terrain. |
| Jul 01, 2000 | GODLEY, TX | N231RR | Minor | substantial | The pilot's inadequate preflight planning and his delay in aborting the takeoff. |
| Jun 29, 2000 | WHITNEY, TX | N6932N | Minor | substantial | The partial loss of engine power, which resulted from the worn carburetor. |
| Jun 03, 2000 | UPLAND, CA | N9207V | Minor | substantial | The failure of the pilot-in-command to maintain directional control of the aircraft on takeoff after the cabin door became ajar. |
| Apr 20, 2000 | MIDDLETOWN, RI | N9187V | Minor | substantial | an inadequate preflight inspection by the pilot which did not detect the water in the fuel tanks prior to departure. |
| Apr 19, 2000 | TOMBALL, TX | N7038V | Minor | substantial | Engine seizure due to the rupture of an oil cooler line. |
| Dec 11, 1999 | READING, PA | N6715U | Minor | substantial | The failure of the number two connecting rod after an improper overhaul by maintenance personnel. |
| Aug 28, 1999 | EMIGRANT GAP, CA | N4201S | Minor | substantial |
The fatigue failure and separation of the number three cylinder due to the cylinder overhaul facility's improper inspection and quality control proces…The fatigue failure and separation of the number three cylinder due to the cylinder overhaul facility's improper inspection and quality control processes. |
| Jul 19, 1999 | MARSHALL, MN | N7141V | Minor | substantial |
the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landi…the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landing attempt by the pilot. |
| Jun 16, 1999 | CANON CITY, CO | N9355M | Minor | destroyed |
The pilot's poor judgement due to his intentional and continued flight into instrument meteorological conditions. Factors were the existing weather co…The pilot's poor judgement due to his intentional and continued flight into instrument meteorological conditions. Factors were the existing weather conditions that included clouds and obscuration. |
| Mar 22, 1999 | IRVING, NY | N5878Q | Minor | substantial | was the pilot's intentional flight into known icing conditions. |