Mooney M20 Safety Record
Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Aug 31, 2012 | Chelan, WA | N132PC | Minor | substantial |
A loss of engine power during climb for reasons that could not be determined because postaccident examination did not reveal any anomalies that would …A loss of engine power during climb for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation. |
| Jul 21, 2012 | Marked Tree, AR | N1310W | Minor | substantial | The loss of engine power during cruise flight due to a malfunction of the fuel injection servo due to a damaged O-ring. |
| May 25, 2012 | Ozark, AR | N2159D | Minor | substantial | The failure of a connecting rod due to oil starvation. |
| May 19, 2012 | Pembroke Pines, FL | N2610W | Minor | substantial | The pilot's improper fuel management, which resulted in a total loss of engine power during approach due to fuel exhaustion. |
| Apr 15, 2012 | Rosamond, CA | N74518 | Minor | substantial | A loss of engine power during takeoff due to fuel starvation as a result of the pilot’s selection of an empty fuel tank prior to departure. |
| Sep 11, 2011 | Kokomo, IN | N9266M | Minor | substantial |
The loss of engine power following takeoff for reasons that could not be determined because postaccident examination did not reveal any anomalies that…The loss of engine power following takeoff for reasons that could not be determined because postaccident examination did not reveal any anomalies that would have precluded normal operation. |
| Aug 30, 2011 | Allen, OK | N5501Q | Minor | substantial | A total loss of engine power in flight due to fuel starvation as a result of the pilot’s inadequate fuel management. |
| Jun 05, 2011 | North Canton, OH | N1146B | Minor | substantial | The pilot’s improper landing flare and recovery from a bounced landing, which resulted in a loss of control. |
| Jan 29, 2011 | Cypress, TX | N64FM | Minor | substantial | The student pilot’s delayed decision to execute a go-around. |
| Oct 13, 2010 | New Smyrna Beach, FL | N5743Q | Minor | substantial | The pilot’s inadequate preflight inspection, which resulted in the loss of engine power due to water contaminated fuel. |
| Jun 04, 2010 | Port Clinton, OH | N1054B | Minor | substantial | The pilot’s delayed decision to abort the landing and his failure to properly reconfigure the airplane during the aborted landing attempt. |
| Jan 17, 2010 | La Veta, CO | N782LU | Minor | substantial | A fuel leak and subsequent fire due to a mechanical defect. |
| Oct 17, 2009 | Hesperia, CA | N1084Z | Minor | substantial | The pilot's improper glide path and failure to maintain clearance from the airport perimeter fence during the landing approach. |
| Oct 10, 2009 | Marathon, FL | N2558Y | Minor | destroyed | A total loss of engine power for undetermined reasons. |
| Sep 17, 2008 | Bolingbrook, IL | N5651Q | Minor | substantial |
The non-mechanical loss of engine power due to the pilot's incorrect positioning of the fuel tank selector prior to takeoff and the subsequent fuel st…The non-mechanical loss of engine power due to the pilot's incorrect positioning of the fuel tank selector prior to takeoff and the subsequent fuel starvation during takeoff. |
| Sep 09, 2008 | Wallace, NC | N21MY | Minor | substantial |
The pilot's failure to abort the takeoff when the engine failed to develop full power. Contributing to the accident was the pilot's failure to remove …The pilot's failure to abort the takeoff when the engine failed to develop full power. Contributing to the accident was the pilot's failure to remove the intake plugs prior to takeoff. |
| Aug 11, 2008 | Ridgeland, SC | N9137V | Minor | substantial | The pilot's inadequate compensation for a crosswind during landing. A factor contributing to the accident was the crosswind. |
| Jul 09, 2008 | Rogers, AR | N7072V | Minor | substantial | The loss of engine power due to fuel exhaustion as a result of the pilot's inadequate in-flight planning/decision. |
| Jun 29, 2008 | Lake Ft Gibson, OK | N1287X | Minor | substantial | The pilot's loss of control while maneuvering the aircraft. |
| Apr 27, 2008 | Howell, MI | N4513H | Minor | substantial |
The inadvertent stall and low airspeed while maneuvering back to the departure airport after the baggage door opened in flight. An additional cause wa…The inadvertent stall and low airspeed while maneuvering back to the departure airport after the baggage door opened in flight. An additional cause was the plot's diverted attention to the opening of the baggage door. |
| Dec 26, 2007 | Sarasota, FL | N5875Q | Minor | substantial | A loss of engine power due to contamination in the fuel filter. |
| Oct 13, 2007 | Muskegon, MI | N1261X | Minor | substantial |
Loss of engine power during initial climb after takeoff for undetermined reasons. A contributing factor was the unsuitable terrain for a forced landi…Loss of engine power during initial climb after takeoff for undetermined reasons. A contributing factor was the unsuitable terrain for a forced landing available to the pilot due to the presence of a residential sub-division and trees. |
| Jul 15, 2007 | Eden Prairie, MN | N4785H | Minor | substantial | The pilot's inability to maintain control of the airplane for undetermined reasons. Contributing to the accident were the embankment and the fence. |
| Apr 16, 2007 | Sidney, OH | N3529H | Minor | substantial |
The total loss of engine power during initial climb due to oil starvation as a result of improper maintenance. The fixed base operator's failure to ad…The total loss of engine power during initial climb due to oil starvation as a result of improper maintenance. The fixed base operator's failure to advise the pilot that the engine had been operated without oil in the engine and soft terrain were factors. |
| Nov 14, 2006 | Akron, OH | N202WB | Minor | substantial |
The pilot's failure to maintain sufficient airspeed during final approach resulting in an inadvertent stall. Contributing factors were the airplane's…The pilot's failure to maintain sufficient airspeed during final approach resulting in an inadvertent stall. Contributing factors were the airplane's low altitude at the time of the stall and the asymmetric flap configuration. |