Mooney M20 Safety Record
Complete NTSB accident and incident history. 1232 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Feb 06, 2001 | PECKVILLE, PA | N1914Y | Incident | substantial | loss of engine power for undetermined reasons. |
| Jan 01, 2001 | Port Huron, MI | N2184N | Incident | substantial |
The pilot failed to maintain directional control of the airplane and the runway selected resulted in a tailwind condition. Factors associated with t…The pilot failed to maintain directional control of the airplane and the runway selected resulted in a tailwind condition. Factors associated with the accident were the gusty crosswind and the snow bank. |
| Nov 27, 2000 | FORT MYERS, FL | N9198V | Incident | substantial | Fuel system contamination that resulted in fuel starvation. |
| Oct 06, 2000 | MONROE, WA | N52202 | Incident | substantial | Oil Pump drive gear shaft separated in shear. A collision with a tree stump during the landing roll was a factor. |
| Sep 10, 2000 | OWASSO, OK | N866B | Incident | substantial | The loss of engine power for undetermined reasons. A factor was the lack of suitable terrain for the forced landing. |
| Sep 09, 2000 | HAILEY, ID | N1024Z | Incident | substantial | The pilot's inadequate compensation for the wind conditions. A crosswind condition was a factor. |
| Aug 03, 2000 | ALBUQUERQUE, NM | N6927U | Incident | substantial | Fuel exhaustion and the pilot's failure the refuel the airplane. Factors were the road signs. |
| Jul 29, 2000 | CANON CITY, CO | N5775Q | Incident | substantial | The pilot's failure to extend the landing gear, which resulted in a wheels up landing. |
| Jul 24, 2000 | ERIE, CO | N5549Q | Incident | substantial | Failure by the pilot to follow procedures and lower the landing gear. |
| Jul 22, 2000 | LONGMONT, CO | N6253U | Incident | substantial |
The pilot's improper fuel tank selector position resulting in fuel starvation and the ditch impacted during the landing roll. A contributing factor w…The pilot's improper fuel tank selector position resulting in fuel starvation and the ditch impacted during the landing roll. A contributing factor was the pilot's failure to follow published procedures and directives. |
| Jul 13, 2000 | ESPANOLA, NM | N201DK | Incident | substantial | The lack of suitable terrain for a forced landing. A factor was a complete loss of power due to mechanical failure. |
| Jun 28, 2000 | TALIHINA, OK | N22166 | Incident | substantial | the partial loss of engine power on takeoff, which resulted from incorrect adjustment of the fuel injector system by maintenance personnel. |
| Jun 08, 2000 | Baker, CA | N31M | Incident | substantial |
The fuel flow became restricted by remnants of fuel tank sealant that had accumulated in the fuel selector screen. Contributing to the pilot's inabil…The fuel flow became restricted by remnants of fuel tank sealant that had accumulated in the fuel selector screen. Contributing to the pilot's inability to restart the engine in flight was the empty fuel tank in the left wing and the fuel gauge indication. The constrained landing area was also a factor. |
| May 11, 2000 | BRYSON CITY, NC | N6998U | Incident | substantial |
The pilot's failure to maintain directional control on landing rollout with a known quartering crosswind, resulting in an on-ground collision with a k…The pilot's failure to maintain directional control on landing rollout with a known quartering crosswind, resulting in an on-ground collision with a known fixed object (wooden pallet.) |
| Apr 05, 2000 | HOUSTON, TX | N8159E | Incident | substantial | The pilot's delayed go-around and his failure to maintain the aircraft's clearance with trees. |
| Jan 21, 2000 | MONTPELIER, VT | N223KT | Incident | substantial |
A blocked crankcase breather line due to ice and improper maintenance which resulted in further restricting the line. A factor in this accident was th…A blocked crankcase breather line due to ice and improper maintenance which resulted in further restricting the line. A factor in this accident was the below freezing outside air temperature. |
| Jan 19, 2000 | TYLER, TX | N1157G | Incident | substantial |
The failure of the crankshaft drive gear as a result of fatigue, which resulted in a forced landing. A factor was the lack of suitable terrain for th…The failure of the crankshaft drive gear as a result of fatigue, which resulted in a forced landing. A factor was the lack of suitable terrain for the forced landing. |
| Sep 09, 1999 | EDNA, TX | N5586Q | Incident | substantial | Fuel exhaustion due to the pilot's inadequate preflight planning. A factor was the lack of suitable terrain for the forced landing. |
| Jul 30, 1999 | MOUNT PLEASANT, TX | N91FH | Incident | substantial | The separation of the fuel line fitting as a result of fatigue. A factors was the lack of suitable terrain for a forced landing. |
| Jul 26, 1999 | HAYWARD, WI | N74523 | Incident | substantial |
the pilot's failure to maintain clearance with the surface of the lake. Factors associated with the accident were the low level flight, dusk light co…the pilot's failure to maintain clearance with the surface of the lake. Factors associated with the accident were the low level flight, dusk light conditions, and the glassy water. |
| Jul 04, 1999 | HARBOR SPRINGS, MI | N201HG | Incident | substantial |
the pilot's inadequate compensation for the wind conditions and his failure to maintain clearance with the trees. Factors associated with the accident…the pilot's inadequate compensation for the wind conditions and his failure to maintain clearance with the trees. Factors associated with the accident were the gusty winds, wind shear, and the trees. |
| Jul 03, 1999 | BIG PINEY, WY | N6253U | Incident | substantial | The pilot's failure to maintain directional control of the aircraft during landing touchdown. A related factor was the gusty crosswind. |
| Jun 29, 1999 | LIBERTY, NC | N7114V | Incident | substantial |
Improper inspection of the muffler assembly resulting in erosion going undetected and the rupture of the muffler and shroud while in cruise flight. Th…Improper inspection of the muffler assembly resulting in erosion going undetected and the rupture of the muffler and shroud while in cruise flight. The condition caused melting of portions of the air induction system, loss of engine power, and the pilot's attempted forced landing that resulted in collision with terrain that sheared one main landing gear and fractured the wheel of the other main landing gear. A factor in the accident was the pilot's obscured vision due to smoke in the cockpit. |
| Jun 05, 1999 | FR | FGJGN | Incident | — | Investigation pending |
| May 28, 1999 | RAVENNA, OH | N496DE | Incident | substantial | The pilot's improper flare which resulted in a hard landing, and his failure to maintain directional control after touchdown. |