Cessna 172N Safety Record
Complete NTSB accident and incident history. 1178 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Aug 15, 2001 | Peyton, CO | N733BW | Serious (1) | substantial |
The pilot's improper go-around procedure and his failure to maintain adequate airspeed which resulted in an inadvertent stall. A factor was the pilot…The pilot's improper go-around procedure and his failure to maintain adequate airspeed which resulted in an inadvertent stall. A factor was the pilot's lack of total experience. |
| Jul 09, 2001 | Caldwell, TX | N7332F | Serious (1) | substantial |
the solo student pilot's intentional engine shutdown, while practicing emergency landing prodecures. A contributing factor was the lack of suitable t…the solo student pilot's intentional engine shutdown, while practicing emergency landing prodecures. A contributing factor was the lack of suitable terrain for the forced landing. |
| Jun 18, 2001 | Richmond Hill, CA | C-GMHU | Serious (1) | substantial | Investigation pending |
| Oct 15, 2000 | JENSEN, UT | N738CW | Serious (1) | substantial |
an undershoot due to misjudging distance/altitude during an emergency landing. Factors were: inadequate preflight, failure to refuel, fuel exhaustion…an undershoot due to misjudging distance/altitude during an emergency landing. Factors were: inadequate preflight, failure to refuel, fuel exhaustion, operating with an inoperative fuel gauge, and failure to attain a proper glide path during approach. |
| May 08, 1999 | LAS VEGAS, NV | CGIUX | Serious (2) | destroyed |
The pilot's premature rotation during the aborted landing and his failure to attain and maintain sufficient airspeed, which resulted in a stall mush. …The pilot's premature rotation during the aborted landing and his failure to attain and maintain sufficient airspeed, which resulted in a stall mush. Factors in the accident were the pilot's decision to attempt a landing in adverse wind conditions beyond the crosswind capability of the airplane and an inoperative stall warning horn system. |
| Apr 29, 1999 | WINTER HAVEN, FL | N739FX | Serious (2) | substantial | The pilot of the other aircraft's failure to maintain visual lookout. A factor was the other pilot's disregard for VFR Traffic pattern procedures. |
| Nov 17, 1998 | CONCORD, NC | N92KK | Serious (1) | substantial |
The pilot's improper in-flight decision and his failure to maintain clearance during approach that resulted in collision with utility lines. Related …The pilot's improper in-flight decision and his failure to maintain clearance during approach that resulted in collision with utility lines. Related factors were dark night, trees and low ceilings. |
| Jul 11, 1998 | LINCOLN, TX | N5632E | Serious (3) | destroyed |
The #3 cylinder exhaust valve rocker arm fulcrum retaining stud backing out of its stud-tapped hole due to the improper tapping of the stud hole by un…The #3 cylinder exhaust valve rocker arm fulcrum retaining stud backing out of its stud-tapped hole due to the improper tapping of the stud hole by unknown maintenance personnel. Contributing factors were the transmission wire, sign and gasoline pump. |
| Dec 16, 1997 | MCKINNEY, TX | N1371E | Serious (3) | substantial |
The pilot's inadequate in-flight/planning decision which resulted in continued flight until fuel exhaustion. Related factors were incorrect fuel gaug…The pilot's inadequate in-flight/planning decision which resulted in continued flight until fuel exhaustion. Related factors were incorrect fuel gauge readings and trees. |
| Jun 26, 1997 | CANTON, MI | N7031Q | Serious (1) | substantial |
A loss of engine power due to fuel starvation from a binding throttle/power lever cable. Also causal was the improper maintenance, installation of th…A loss of engine power due to fuel starvation from a binding throttle/power lever cable. Also causal was the improper maintenance, installation of the throttle arm. Contributing to the accident were the dark night and unsuitable terrain for the forced landing. |
| Apr 04, 1997 | AVALON, CA | N733CN | Serious (2) | destroyed |
The pilot's misjudging the airplane's altitude and distance to the runway and an excessive descent rate, which led to an undershoot, and the pilot's f…The pilot's misjudging the airplane's altitude and distance to the runway and an excessive descent rate, which led to an undershoot, and the pilot's failure to maintain an adequate airspeed during the approach. Contributing factors were the pilot's delay in initiating corrective action. |
| Feb 07, 1997 | MADRAS, OR | N5618J | Serious (2) | substantial |
The pilot's inadvertent visual flight rules (VFR) flight into instrument meteorological conditions (IMC). Factors include the pilot's improper decisio…The pilot's inadvertent visual flight rules (VFR) flight into instrument meteorological conditions (IMC). Factors include the pilot's improper decision to fly under a low ceiling while in mountainous/hilly terrain, and his encounter with fog and low clouds while maneuvering in a narrow canyon. |
| Feb 23, 1996 | AUSTIN, TX | N6601D | Serious (2) | substantial | the partial loss of engine power due to the failure of the #3 connecting rod. A factor was the lack of suitable terrain for the forced landing. |
| Sep 08, 1995 | GLENNALLEN, AK | N737SP | Serious (1) | substantial |
Improper planning/decision by the pilot, which resulted in fuel exhaustion, due to an inadequate supply of fuel. A factor relating to the accident wa…Improper planning/decision by the pilot, which resulted in fuel exhaustion, due to an inadequate supply of fuel. A factor relating to the accident was: the lack of suitable terrain for an emergency landing. |
| Sep 01, 1995 | COLORADO SPGS, CO | N4814F | Serious (2) | destroyed |
BLOCKAGE OF THE CARBURETOR BY A PIECE OF FOREIGN MATERIAL, WHICH RESULTED IN A LOSS OF ENGINE POWER, AND FAILURE OF THE PILOT TO MAINTAIN AIRSPEED, WH…BLOCKAGE OF THE CARBURETOR BY A PIECE OF FOREIGN MATERIAL, WHICH RESULTED IN A LOSS OF ENGINE POWER, AND FAILURE OF THE PILOT TO MAINTAIN AIRSPEED, WHICH RESULTED IN AN INADVERTENT STALL. THE HIGH DENSITY ALTITUDE AND THE PILOT'S FAILURE TO PROPERLY LEAN THE FUEL MIXTURE WERE POSSIBLE FACTORS. |
| Jul 25, 1995 | KILL DEVIL HILL, NC | N5415J | Serious | — | The attempt by the pilots to perform the unfamiliar procedure of starting the airplane's engine by hand. |
| Aug 21, 1994 | SIMI VALLEY, CA | N739VY | Serious | substantial |
FUEL EXHAUSTION AFTER THE STUDENT PILOT BECAME LOST/DISORIENTED. FACTORS RELATED TO THE ACCIDENT WERE: FAILURE OF THE SUPERVISING FLIGHT INSTRUCTOR (…FUEL EXHAUSTION AFTER THE STUDENT PILOT BECAME LOST/DISORIENTED. FACTORS RELATED TO THE ACCIDENT WERE: FAILURE OF THE SUPERVISING FLIGHT INSTRUCTOR (CFI) TO FOLLOW THE FAA APPROVED SYLLABUS, INADEQUATE SUPERVISION BY THE COMPANY/OPERATOR MANAGEMENT, DARKNESS, AND THE STUDENT'S LACK OF NIGHT FLYING EXPERIENCE. |
| Jul 04, 1994 | PRINCESS ANNE, MD | N4828G | Serious (1) | substantial |
THE PILOT'S FAILURE TO DO A GO-AROUND AND HER DELAY IN THE INITIATING OF AN ABORTED LANDING, WHICH RESULTED IN HER FAILURE TO OUTCLIMB TREES DURING TH…THE PILOT'S FAILURE TO DO A GO-AROUND AND HER DELAY IN THE INITIATING OF AN ABORTED LANDING, WHICH RESULTED IN HER FAILURE TO OUTCLIMB TREES DURING THE ABORTED LANDING. |
| Jun 30, 1994 | SCHURZ, NV | N733AA | Serious (1) | destroyed | the pilot's inability to maintain an adequate airspeed in the takeoff initial climb due to an encounter with a windshear. |
| Apr 03, 1994 | GASQUET, CA | N6290D | Serious (1) | destroyed | THE FAILURE OF THE PILOT TO ADEQUATELY COMPENSATE FOR THE CROSS- WIND CONDITIONS, AND TO MAINTAIN PROPER ALIGNMENT WITH THE RUNWAY. |
| Mar 04, 1994 | PRESCOTT, AZ | N487ER | Serious (2) | substantial |
THE STUDENT PILOT'S DELAYED FLARE AND FAILURE TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRCRAFT, AND THE FLIGHT INSTRUCTOR'S INADEQUATE SUPERVISION OF T…THE STUDENT PILOT'S DELAYED FLARE AND FAILURE TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRCRAFT, AND THE FLIGHT INSTRUCTOR'S INADEQUATE SUPERVISION OF THE FLIGHT. |
| Nov 15, 1993 | FORT COLLINS, CO | N4829E | Serious (1) | destroyed |
POWER LOSS DUE TO THROTTLE LINKAGE DISCONNECT. FACTORS WERE MISSING COTTER KEY, IMPROPER MAINTENANCE, AND THE LACK OF SUITABLE TERRAIN FOR THE FORCED …POWER LOSS DUE TO THROTTLE LINKAGE DISCONNECT. FACTORS WERE MISSING COTTER KEY, IMPROPER MAINTENANCE, AND THE LACK OF SUITABLE TERRAIN FOR THE FORCED LANDING. |
| Aug 07, 1993 | LEEDS, ME | N739EP | Serious (1) | substantial | The loss of engine power for undetermined reasons. |
| Jul 23, 1993 | LONG GROVE, IL | N733XS | Serious (4) | substantial |
THE PILOT-IN-COMMAND'S FAILURE TO REFUEL THE AIRPLANE PRIOR TO FUEL EXHAUSTION. RELATED FACTORS TO THE ACCIDENT WERE: INADEQUATE CERTIFICATION/APPROVA…THE PILOT-IN-COMMAND'S FAILURE TO REFUEL THE AIRPLANE PRIOR TO FUEL EXHAUSTION. RELATED FACTORS TO THE ACCIDENT WERE: INADEQUATE CERTIFICATION/APPROVAL OF THE STC BY THE FAA, INADEQUATE PERFORMANCE DATA, AND UNAVAILABLE FUEL CONSUMPTION INFORMATION. |
| May 08, 1993 | FALMOUTH, KY | N1329E | Serious (2) | substantial |
THE PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRPLANE DURING THE LANDING ROLL, WHICH RESULTED IN AN INADVERTENT SWERVE, AND HIS DELAYED …THE PILOT'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL OF THE AIRPLANE DURING THE LANDING ROLL, WHICH RESULTED IN AN INADVERTENT SWERVE, AND HIS DELAYED REMEDIAL ACTION. |