Cessna 172N Safety Record
Complete NTSB accident and incident history. 1178 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Oct 08, 2001 | Colo Springs, CO | N2364E | Incident | substantial | the pilot's inadequate landing flare, which resulted in a hard landing. A contributing factor was the pilot's excessive airspeed on final approach. |
| Oct 06, 2001 | Beaver Island, MI | N73630 | Incident | substantial | The pilot not maintaining directional control of the airplane during landing. The gusty crosswind and the berm were factors. |
| Sep 14, 2001 | Sarasota, FL | N19SC | Incident | substantial |
The pilot's improper in-flight decision to land at an airport with high wind conditions, which resulted in a loss of control on the ground during taxi…The pilot's improper in-flight decision to land at an airport with high wind conditions, which resulted in a loss of control on the ground during taxi operations and subsequent nose over of the airplane. |
| Sep 08, 2001 | Pasco, WA | N426SK | Incident | substantial |
The DHC-8 maintenance crew's failure to maintain radio contact with the tower during its engine run. Factors included the tower controller not issuin…The DHC-8 maintenance crew's failure to maintain radio contact with the tower during its engine run. Factors included the tower controller not issuing a safety advisory on the DHC-8 engine run to the accident pilot as recommended by FAA guidance, and the FAA's failure to make information on jet blast/prop blast hazards available to controllers. |
| Jul 27, 2001 | Farmington, NM | N181SP | Incident | destroyed |
the pilot's failure to maintain clearance from the powerline while descending for an emergency landing. A contributing factor was the loss of engine p…the pilot's failure to maintain clearance from the powerline while descending for an emergency landing. A contributing factor was the loss of engine power for an undetermined reason. |
| Jul 10, 2001 | West Chicago, IL | N5285E | Incident | substantial |
The instructor pilot's inadequate recovery from the bounced landing and inadequate supervision of the dual students alignment with the runway. A fact…The instructor pilot's inadequate recovery from the bounced landing and inadequate supervision of the dual students alignment with the runway. A factor was the student pilot not maintaining proper alignment with the runway during landing. |
| Jul 01, 2001 | Boulder City, NV | N737SH | Incident | substantial | the loss of engine power while in cruise flight due to the mechanic's improper magneto timing. |
| Jun 17, 2001 | Colquitt, GA | N75579 | Incident | substantial |
The student pilot's failure to use the fuel selector valve properly which resulted in fuel starvation and the subsequent loss of engine power, and the…The student pilot's failure to use the fuel selector valve properly which resulted in fuel starvation and the subsequent loss of engine power, and the pilot's improper flare during landing. |
| Mar 14, 2001 | SHOW LOW, AZ | N738PP | Incident | substantial | The pilot's failure to maintain directional control resulting in an encounter with terrain and a nose over. |
| Feb 15, 2001 | San Diego, CA | N4922D | Incident | substantial | The pilot's failure to maintain directional control of the airplane during landing rollout. |
| Jan 01, 2001 | Lincoln, IL | N737WQ | Incident | substantial |
The pilot's failure to maintain directional control on the runway. Factors relating to this accident were the aborted takeoff attempt, the pilot's im…The pilot's failure to maintain directional control on the runway. Factors relating to this accident were the aborted takeoff attempt, the pilot's improper in-flight planning/decision, and the snowbank. |
| Dec 30, 2000 | Elkhart, IN | N6326F | Incident | substantial |
The loss of directional control by the student pilot and the inadequate remedial action and inadequate supervision by the certified flight instructor.…The loss of directional control by the student pilot and the inadequate remedial action and inadequate supervision by the certified flight instructor. Factors were the snow and ice covered runway and the snowbank. |
| Nov 30, 2000 | MARANA, AZ | N8173E | Incident | substantial |
The student pilot's improper flare and improper recovery from a bounced landing. A factor in the accident was the morning sun, which momentarily rest…The student pilot's improper flare and improper recovery from a bounced landing. A factor in the accident was the morning sun, which momentarily restricted the pilot's vision. |
| Nov 03, 2000 | SPANGLE, WA | N734UW | Incident | substantial |
The pilot's inadequately executed remedial action and his failure to ensure that the aircraft touched down at the proper location. Factors include a d…The pilot's inadequately executed remedial action and his failure to ensure that the aircraft touched down at the proper location. Factors include a dark night, an unlighted runway, and trees off the approach end of the runway. |
| Sep 03, 2000 | NORTH LAS VEGAS, NV | N739HA | Incident | substantial |
The failure of the pilot-in-command to maintain proper airspeed during the aborted landing go-around which resulted in a stall/mush and impact with te…The failure of the pilot-in-command to maintain proper airspeed during the aborted landing go-around which resulted in a stall/mush and impact with terrain. |
| Jun 30, 2000 | DURANGO, CO | N4642J | Incident | substantial |
The pilot prematurely flaring the airplane for landing, resulting in a hard landing, followed by an inadvertent pilot-induced porpoise and loss of dir…The pilot prematurely flaring the airplane for landing, resulting in a hard landing, followed by an inadvertent pilot-induced porpoise and loss of directional control. A factor was the fence. |
| Jun 29, 2000 | SAN ANTONIO, TX | N4918G | Incident | substantial |
The flight instructor's failure to refuel the airplane, which resulted in fuel exhaustion. Contributing factors were the flight instructor's fatigued…The flight instructor's failure to refuel the airplane, which resulted in fuel exhaustion. Contributing factors were the flight instructor's fatigued condition and diverted attention. |
| Jun 26, 2000 | CANTON, MI | N3416E | Incident | substantial |
the CFI delayed initiating a go-around during the landing. Factors associated with the accident were the student pilot's inadequate handling of the ai…the CFI delayed initiating a go-around during the landing. Factors associated with the accident were the student pilot's inadequate handling of the airplane, the crosswind condition, and the soft terrain on which the airplane touched down. |
| Jun 24, 2000 | ATLANTIC OCEAN, AO | N738WD | Incident | substantial | Loss of engine power for undetermined reasons. A factor was the pilot failed to use carburetor heat during the descent. |
| Jun 23, 2000 | GREENVILLE, IL | N4919G | Incident | substantial |
the student pilot failed to properly flare the airplane while landing. A factor associated with the accident was the student pilot's lack of total ex…the student pilot failed to properly flare the airplane while landing. A factor associated with the accident was the student pilot's lack of total experience. |
| Jun 22, 2000 | SANTA ANA, CA | N7598D | Incident | substantial |
The loss of engine power during the initial takeoff climb, at too low an altitude to afford remedial action, because of an ingested valve, and the air…The loss of engine power during the initial takeoff climb, at too low an altitude to afford remedial action, because of an ingested valve, and the airplane's subsequent collision with the ground adjacent to the runway. |
| May 27, 2000 | LINCOLNTON, NC | N734ZD | Incident | substantial |
The inadequate supervision of the student pilot by the CFI for his failure to note that the student was performing a go-around from a low pass with 30…The inadequate supervision of the student pilot by the CFI for his failure to note that the student was performing a go-around from a low pass with 30-degree of flaps extended instead of the POH recommended 20-degrees. A factor in the accident was the failure of the student to retract the flaps from 40 degrees to 20 degrees during the go-around from a low pass. |
| May 17, 2000 | ATLANTIC OCEAN, AO | N738VZ | Incident | destroyed | A loss of engine power for undetermined reasons. |
| Apr 13, 2000 | CHESTERFIELD, MO | N5909E | Incident | substantial | the pilot misjudged the landing flare which resulted in the airplane porpoising on the runway during the landing. |
| Apr 11, 2000 | LAKEPORT, CA | N6104G | Incident | substantial |
The pilot's decision to continue with a high, steep, and fast approach, which resulted in a touchdown beyond the halfway point of the runway and the i…The pilot's decision to continue with a high, steep, and fast approach, which resulted in a touchdown beyond the halfway point of the runway and the inability to stop on the remaining pavement, and, his delayed decision to initiate a landing abort. Also causal was the pilot's failure to retract the flaps to the go around/aborted landing position. |