Boeing 737 Safety Record

Complete NTSB accident and incident history. 1188 events recorded from 1982 to 2026.

1188

All Events

501

Incidents

64

Minor

190

Serious

46

Fatal (3137 fatalities)

Date Location Reg# Severity Damage Probable Cause
Jun 29, 1995 ELKO, NV N457TM Incident minor in-flight separation of the aileron as a result of inadequate bonding.
May 19, 1995 TALLAHASSEE, FL N60312 Serious (1)
THE FAILURE OF A PASSENGER TO COMPLY WITH FLIGHT CREW INSTRUCTIONS TO REMAIN SEATED WITH HER SEAT BELT FASTENED WHICH RESULTED IN HER BEING INJURED WH…

THE FAILURE OF A PASSENGER TO COMPLY WITH FLIGHT CREW INSTRUCTIONS TO REMAIN SEATED WITH HER SEAT BELT FASTENED WHICH RESULTED IN HER BEING INJURED WHILE WALKING IN THE AISLE DURING A TURBULENCE ENCOUNTER.

Apr 14, 1995 DENVER, CO EICEU Incident substantial
PROPER DESCENT RATE NOT MAINTAINED BY THE FIRST OFFICER, RESULTING IN A HARD LANDING. FACTORS WERE UNFAVORABLE WIND CONDITIONS AND THE CAPTAIN'S INADE…

PROPER DESCENT RATE NOT MAINTAINED BY THE FIRST OFFICER, RESULTING IN A HARD LANDING. FACTORS WERE UNFAVORABLE WIND CONDITIONS AND THE CAPTAIN'S INADEQUATE SUPERVISION OF THE FIRST OFFICER.

Apr 07, 1995 CHICAGO, IL N9090U Incident minor
the inadequacy or deterioration of lubricating grease in the wheel bearing, which led to the total bearing failure and subsequent loss of the wheel. …

the inadequacy or deterioration of lubricating grease in the wheel bearing, which led to the total bearing failure and subsequent loss of the wheel. Factors were the insufficiently defined procedures for repacking the bearing, along with an insufficient method of retaining lubricant within the bearing.

Feb 01, 1995 SAN PAULO, BR PPSMV Incident Investigation pending
Jan 27, 1995 DALLAS, TX N71SW Serious (1) THE FLIGHT ATTENDANTS' LACK OF SUPERVISION OF DEPLANING PASSENGERS. A FACTOR WAS LACK OF SUPERVISION BY ACCIDENT VICTIMS MOTHER.
Jan 24, 1995 ALBUQUERQUE, NM N155AW Incident
maintenance personnel inadvertently overservicing the left main landing gear strut with nitrogen that, during rotation with the aircraft weight on the…

maintenance personnel inadvertently overservicing the left main landing gear strut with nitrogen that, during rotation with the aircraft weight on the strut reduced, gave the pilots a rolling sensation to the right.

Jan 19, 1995 ATLANTA, GA N4515W Incident minor
THE INADEQUATE INSPECTION OF THE AIRCRAFT BY OTHER MAINTENANCE PERSONNEL, IN THAT THEY DID NOT PROPERLY DIAGNOSE DISCREPANCIES IN THE ANTISKID BRAKING…

THE INADEQUATE INSPECTION OF THE AIRCRAFT BY OTHER MAINTENANCE PERSONNEL, IN THAT THEY DID NOT PROPERLY DIAGNOSE DISCREPANCIES IN THE ANTISKID BRAKING SYSTEM.

Jan 01, 1995 HOUSTON, TX N326SW Incident ENCOUNTER WITH WAKE TURBULENCE.
Dec 29, 1994 VAN, TU TCJES Incident destroyed Investigation pending
Dec 11, 1994 ANCHORAGE, AK N681MA Serious (1) THE FAILURE OF THE B SYSTEM CHANNEL AUTOPILOT ELEVATOR ACTUATOR.
Sep 19, 1994 ATLANTIC OCEAN, AO N433US Serious (1) THE INFLIGHT ENCOUNTER WITH TURBULENCE IN CLOUDS.
Jul 07, 1994 SOUTH BEND, IN N60SW Serious (1) THE ENCOUNTER WITH UNFORCASTED AND UNREPORTED TURBULENCE.
Apr 27, 1994 HONOLULU, HI N804AL Minor The failure of the battery transfer relay resulting in multiple system failures.
Feb 10, 1994 CHICAGO, IL N408PE Incident minor
AN INADEQUATE PROCEDURE FOR HANDLING OF WHEEL CHOCKS BY COMPANY MAINTENANCE AND OPERATIONS PERSONNEL. FACTORS ASSOCIATED WITH THIS ACCIDENT WERE AN IN…

AN INADEQUATE PROCEDURE FOR HANDLING OF WHEEL CHOCKS BY COMPANY MAINTENANCE AND OPERATIONS PERSONNEL. FACTORS ASSOCIATED WITH THIS ACCIDENT WERE AN INADEQUATE INSPECTION OF THE AIRPLANE BY COMPANY MAINTENANCE PERSONNEL, AND AN INADEQUATE PRE-FLIGHT INSPECTION BY THE CO-PILOT.

Jan 19, 1994 LITTLE ROCK, AR N53SW Incident minor WAS THE LANDING GEAR SEPARATION DUE TO AN UNDETERMINED CAUSE.
Dec 08, 1993 DFW AIRPORT, TX N166AW Incident minor A FAILURE BY THE PILOT-IN-COMMAND TO ATTAIN A STABILZED APPROACH. FACTORS WERE THE FOG AND FAILURE OF THE COPILOT TO MONITOR THE APPROACH.
Sep 21, 1993 INDIANAPOLIS, IN N527AU Incident an undetermined problem which resulted in the physical impairment of flight attendants, passengers and the first officer.
Sep 08, 1993 ST. LOUIS, MO N350SW Incident minor a failure of the left outboard foreflap due to the loss of the bolts that hold the inboard sequencing carriage to the foreflap attach lug.
Jun 07, 1993 ANCHORAGE, AK N673MA Incident minor THE FAILURE OF THE NOSE LANDING GEAR INNER CYLINDER FROM AN OVERLOAD/OVERSTRESS CONDITION.
Apr 24, 1993 DENVER, CO N905UA Incident
THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN ADEQUATE SEPARATION FROM THE BOEING 757, AND HIS FAILURE TO STAY ABOVE THE PROBABLE PATH OF THE BOEING'S WA…

THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN ADEQUATE SEPARATION FROM THE BOEING 757, AND HIS FAILURE TO STAY ABOVE THE PROBABLE PATH OF THE BOEING'S WAKE VORTICES, WHICH RESULTED IN THE VORTEX ENCOUNTER. FACTORS RELATED TO THE ACCIDENT WERE: THE CROSSWIND, AND AN INADEQUACY IN ATC PROCEDURES CONCERNING VISUAL APPROACHES OF AIRCRAFT, BEHIND AND DOWNWIND FROM APPROACHES OF HEAVIER AIRCRAFT TO PARALLEL OR ADJACENT RUNWAYS.

Mar 15, 1993 NEWARK, NJ N14212 Incident
INADEQUATE MAINTENANCE/INSPECTION BY COMPANY MAINTENANCE PERSONNEL, THE MANUFACTURER'S INADEQUATE INSPECTION AND/OR REPLACEMENT PROCEDURES FOR THE AIL…

INADEQUATE MAINTENANCE/INSPECTION BY COMPANY MAINTENANCE PERSONNEL, THE MANUFACTURER'S INADEQUATE INSPECTION AND/OR REPLACEMENT PROCEDURES FOR THE AILERON CABLES, AND SUBSEQUENT FAILURE OF THE 'DOWN' AILERON CONTROL CABLE DUE TO WEAR.

Feb 13, 1993 PORTLAND, ME N403PE Incident
THE PILOT IN COMMAND'S EXCESSIVE AIRSPEED DURING APPROACH, AND HIS FAILURE TO FOLLOW THE PROPER BRAKING PROCEDURES DURING LANDING AS PER COMPANY TRAIN…

THE PILOT IN COMMAND'S EXCESSIVE AIRSPEED DURING APPROACH, AND HIS FAILURE TO FOLLOW THE PROPER BRAKING PROCEDURES DURING LANDING AS PER COMPANY TRAINING. FACTORS CONTRIBUTING TO THE ACCIDENT INCLUDE A TAILWIND AND A WET, DOWNHILL RUNWAY.

Dec 08, 1992 FLUSHING, NY N516AU Fatal
A LACK OF ADEQUATE CLEARANCE BETWEEN THE WALKER AND TUG WHICH RESULTED IN THE WALKER BEING STRUCK BY THE TUG WHEN HE FELL FOR UNKNOWN REASON(S). A FA…

A LACK OF ADEQUATE CLEARANCE BETWEEN THE WALKER AND TUG WHICH RESULTED IN THE WALKER BEING STRUCK BY THE TUG WHEN HE FELL FOR UNKNOWN REASON(S). A FACTOR RELATED TO THE ACCIDENT WAS THE LACK OF A POLICY TO STAY CLEAR OF THE TUG, TOWBAR, AND NOSEWHEEL OF THE AIRPLANE, WHILE PUSHBACK OPERATIONS ARE IN MOTION.

Nov 21, 1992 SAN LUIS, AR LVJNE Incident destroyed Investigation pending
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
← Boeing 737 For Sale All Boeing Models
Data source: NTSB Aviation Accident Database · About our data
View 2 Boeing 737 for sale ↓