Boeing 737 Safety Record

Complete NTSB accident and incident history. 1188 events recorded from 1982 to 2026.

1188

All Events

501

Incidents

64

Minor

190

Serious

46

Fatal (3137 fatalities)

Date Location Reg# Severity Damage Probable Cause
Sep 12, 1999 LOS ANGELES, CA N388UA Incident substantial
The lavatory service driver's failure to follow established company procedures and directives. A factor in the accident was the airline's use of a on…

The lavatory service driver's failure to follow established company procedures and directives. A factor in the accident was the airline's use of a one person pushback procedure.

Sep 02, 1999 SANTA BARBARA, CA N371UA Serious (1) minor The flight's encounter with wake vortices from a preceding heavy aircraft.
Aug 31, 1999 BA, AR LVWRZ Fatal (80) Investigation pending
Aug 26, 1999 DURBAN, SF UNK Incident Investigation pending
Jul 08, 1999 ATLANTIC OCEAN, AO N12221 Serious (1) minor the aircrew's inadvertent encounter with unforecast clear air turbulence.
Jun 26, 1999 LAFAYETTE, LA N650SW Serious (1) The pilot's inadvertent flight into an adverse weather condition. A factor was the turbulence.
Jun 09, 1999 ZHANJIANG, CH B2525 Minor substantial Investigation pending
May 25, 1999 NEWARK, NJ N16703 Serious (1) In flight encounter with turbulence which caused a flight attendant to fall and break two bones in his right leg.
May 06, 1999 CHICAGO, IL N208AU Serious (1)
the flight attendants did not follow the cockpit crews instructions to be seated because of expected turbulence. A factor associated with the acciden…

the flight attendants did not follow the cockpit crews instructions to be seated because of expected turbulence. A factor associated with the accident was the turbulence encountered.

Apr 07, 1999 CEYHAN ADANA, TU TC-JEP Fatal (6) destroyed Investigation pending
Mar 17, 1999 NEWARK, NJ N17321 Serious (1) The flight attendant's failure to follow cabin door opening procedures.
Mar 04, 1999 BIARRITZ, FR FGBYA Incident substantial Investigation pending
Dec 15, 1998 ORLANDO, FL N327DL Incident minor
A discharged battery due to a loss of electrolyte, and the latent shorted failures of the No. 1 and 2 generator control unit (GCU) blocking diodes (CR…

A discharged battery due to a loss of electrolyte, and the latent shorted failures of the No. 1 and 2 generator control unit (GCU) blocking diodes (CR910) for undetermined reasons. These failures resulted in an excessive current drawn from both GCUs, during the flight crew's attempt to start the auxiliary power unit, that caused the immediate overload (opening) of the AC power supply input fuses (POR fuses) internal to each GCU, and subsequent loss of the No.1 and 2 generators; complete discharge of the battery, and subsequent total loss of electrical power. Contributing to the incident was the incorrect reading of the cockpit DC voltmeter (read higher than actual reading) allowing the flight crew to depart with an unreliable (discharged) battery.

Dec 14, 1998 SACRAMENTO, CA N328AW Serious (1) The failure of the second and third flight attendants to comply with instructions to remain seated in anticipation of turbulence.
Dec 08, 1998 NEW YORK, NY GCPX Incident
The Cessna pilot's incorrect visual identification of the Boeing 737's altitude, and decision to take evasive action that was not required, which resu…

The Cessna pilot's incorrect visual identification of the Boeing 737's altitude, and decision to take evasive action that was not required, which resulted in the two airplanes coming within 500 feet horizontally, and 0 feet vertically of one another.

Nov 06, 1998 NEWARK, NJ N12318 Incident minor
A loss of torque on the apex nut of the shimmy damper for undetermined reason(s), which resulted in a failure of the shimmy damper, and the subsequent…

A loss of torque on the apex nut of the shimmy damper for undetermined reason(s), which resulted in a failure of the shimmy damper, and the subsequent failure of the lower torsion link of the right main landing gear.

Nov 01, 1998 ATLANTA, GA EICJW Minor substantial
(1) the capping of the incorrect hydraulic line by mechanics, which led to the failure of hydraulic system A; (2) the mechanics' lack of experience wo…

(1) the capping of the incorrect hydraulic line by mechanics, which led to the failure of hydraulic system A; (2) the mechanics' lack of experience working with the Boeing 737 hydraulic system; and (3) the maintenance controller's failure to ascertain more information regarding the leaking hydraulic line before instructing the mechanics to cap the line and deactivate the right thrust reverser. Contributing to the cause of the accident were (1) the asymmetric directional control resulting from the deactivation of the right thrust reverser; (2) the depletion of the left and right inboard brake accumulator pressure because of the flight crew's use of the rudder pedals with only the left thrust reverser to control the direction of the airplane down the runway; (3) the failure of the right outboard brake because the airplane was slowed without the use of the left and right inboard brakes and was traveling at a higher-than-normal speed and with heavy gross weight; (4) the failure of the right outboard brake after one of the right outboard pistons overtraveled and unported its o-ring, allowing system B hydraulic fluid to deplete and the left outboard brake to fail; and (5) the mechanics' improper use of the illustrated parts catalog for maintenance and troubleshooting and the maintenance controller's failure to use the appropriate documents for maintenance and troubleshooting.

Sep 17, 1998 GUADALAJARA, MX N20643 Incident Investigation pending
Aug 14, 1998 JUNEAU, AK N799AS Incident substantial The flight crew's inadequate recovery from a bounced landing.
Aug 13, 1998 GATWICK, UK GSBEB Incident Investigation pending
Aug 07, 1998 MCCONNELLSBURG, PA N515AU Minor minor A high altitude encounter with wake vortices.
Jul 07, 1998 BIRMINGHAM, AL N701GS Incident minor
The improper electronic control unit software logic that permitted the electronic control unit to lock on a failed hydromechanical resolver, which fai…

The improper electronic control unit software logic that permitted the electronic control unit to lock on a failed hydromechanical resolver, which failed due to damage to a wire that was incurred during the manufacturing process, resulting in an uncommanded and sudden increase in fuel flow to the engine that damaged the turbine and caused the engine to lose power.

Jul 02, 1998 BRAZIL, BR PTTEN Incident Investigation pending
Jun 27, 1998 MUNICH, GE DAHFD Incident Investigation pending
Jun 20, 1998 MARSEILLES, FR FGIXP Incident Investigation pending
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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