Boeing 737 Safety Record
Complete NTSB accident and incident history. 1188 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 14, 2011 | Cuenca, EC | HC-CJB | Incident | minor | Investigation pending |
| May 12, 2011 | Atlanta, GA | N308DE | Incident | substantial | The B737-700 pilot did not maintain adequate wing tip clearance while taxiing around the stopped B-737-800. |
| May 06, 2011 | Greenville, MS | N12221 | Incident | substantial |
The failure of a utility pipe beneath the ramp surface, which caused a localized void in the soil and resulting reduction in the load bearing capabili…The failure of a utility pipe beneath the ramp surface, which caused a localized void in the soil and resulting reduction in the load bearing capability of the ramp. |
| Apr 26, 2011 | Chicago, IL | N799SW | Incident | minor |
The flight crew's delayed deployment of the speedbrakes and thrust reversers, resulting in insufficient runway remaining to bring the airplane to a st…The flight crew's delayed deployment of the speedbrakes and thrust reversers, resulting in insufficient runway remaining to bring the airplane to a stop. Contributing to the delay in deployment of these stopping devices was the flight crew's inadequate monitoring of the airplane's configuration after touchdown, likely as a result of being distracted by a perceived lack of wheel braking effectiveness. Contributing to the incident was the flight crew's omission of the Before Landing checklist, which includes an item to verify speedbrake arming before touchdown, as a result of workload and operational distractions during the approach phase of flight. |
| Apr 25, 2011 | Stockholm, SW | EI-DAD | Incident | — | Investigation pending |
| Apr 01, 2011 | Yuma, AZ | N632SW | Minor | substantial |
the improper installation of the fuselage crown skin panel at the S-4L lap joint during the manufacturing process, which resulted in multiple site dam…the improper installation of the fuselage crown skin panel at the S-4L lap joint during the manufacturing process, which resulted in multiple site damage fatigue cracking and eventual failure of the lower skin panel. Contributing to the injuries was flight attendant A's incorrect assessment of his time of useful consciousness, which led to his failure to follow procedures requiring immediate donning of an oxygen mask when cabin pressure is lost. |
| Mar 30, 2011 | Dayton, OH | N360WA | Incident | substantial |
The flightcrew's inadequate preflight inspection, resulting in in-flight structural damage to the airplane's fuselage from an unsecured pallet jack th…The flightcrew's inadequate preflight inspection, resulting in in-flight structural damage to the airplane's fuselage from an unsecured pallet jack that was located in the airplane's empty cargo hold. |
| Mar 13, 2011 | Toronto, CA | C-FTAH | Incident | — | Investigation pending |
| Feb 21, 2011 | Southlake, TX | N945AN | Incident | minor | The tractor driver’s failure to confirm that the tow bar head/handle was secured correctly to the airplane. |
| Feb 21, 2011 | Casablanca, Morocco, MO | CN-ROR | Incident | — | Investigation pending |
| Feb 15, 2011 | Pekanbaru, ID | PK-LHH | Incident | minor | <br /><br /> |
| Feb 14, 2011 | Pekanbaru, ID | PK-LFI | Incident | minor | <br /><br /> |
| Jan 14, 2011 | Vilnius, LH | ES-ABL | Incident | — | Investigation pending |
| Jan 10, 2011 | Montpelier, FR | F-GIXD | Incident | — | <br /><br /> |
| Jan 03, 2011 | Los Angeles, CA | N831NN | Incident | substantial |
the early rotation of the airplane to an angle at which the fuselage contacted the runway. Contributing to early rotation was the Captain’s react…the early rotation of the airplane to an angle at which the fuselage contacted the runway. Contributing to early rotation was the Captain’s reaction to the erroneous V1 automated callout, likely assuming that the airplane was at or close to the correct Vr at the same time. The erroneous automated callout was likely due to a keystroke entry error by the FO when manually entering takeoff data for a newly assigned departure runway. |
| Dec 25, 2010 | San Francisco, CA | N248WN | Incident | — |
The probable cause of the undercowl in-flight engine fire was the insufficient installation torque of the bolts that secure the fuel manifold cover to…The probable cause of the undercowl in-flight engine fire was the insufficient installation torque of the bolts that secure the fuel manifold cover to the fuel manifold. Engine vibrations and fuel pressure cycles caused the bolts to gradually loosen further until one bolt lost all its tightening torque and fell out. The internal fuel pressure then forced open the fuel manifold cover at the location of the missing bolt, causing a gap between the two mating surfaces which allowed fuel to push past the integral packing, resulting in a fuel leak onto the hot engine cases where it ignited resulting in a fire. |
| Dec 18, 2010 | Philadelphia, PA | N650SW | Incident | substantial | the failure of the ground operations personnel to maintain awareness of the relative position of the two airplanes. |
| Dec 13, 2010 | Rio De Janiero, BR | PR-WJO | Incident | — | <br /><br /> |
| Dec 09, 2010 | Covington, KY | N3731T | Incident | — | The local controller's distraction with a helicopter south of the field. |
| Dec 01, 2010 | Montreal, CA | N901AN | Incident | minor | <br /><br /> |
| Nov 04, 2010 | Puerto Vallerta, MX | XA-UHY | Incident | minor | Investigation pending |
| Oct 29, 2010 | Fort Lauderdale, FL | C-FWAQ | Incident | substantial | The ground service vehicle driver's depressing of the accelerator rather than the brake pedal, resulting in a collision with the airplane. |
| Oct 02, 2010 | Amsterdam, NL | TC-TJF | Incident | — | Investigation pending |
| Sep 20, 2010 | Budapest, HU | HA-LOE | Incident | — | Investigation pending |
| Aug 23, 2010 | London, UK | LN-RPH | Serious (1) | — | Investigation pending |