Boeing 737 Safety Record

Complete NTSB accident and incident history. 1188 events recorded from 1982 to 2026.

1188

All Events

501

Incidents

64

Minor

190

Serious

46

Fatal (3137 fatalities)

Date Location Reg# Severity Damage Probable Cause
Jul 02, 2000 ORLANDO, FL N460PR Incident substantial
The captain's failure to stop the aircraft when given a stop signal by the ground marshaller and his failure to turn the aircraft when given a turn si…

The captain's failure to stop the aircraft when given a stop signal by the ground marshaller and his failure to turn the aircraft when given a turn signal by the ground marshaller as he taxied into the gate resulting in the aircraft's left wing colliding with ground equipment.

Jan 02, 2000 AMSTERDAM, NL PHHVV Incident minor Investigation pending
Dec 24, 1999 SALT LAKE CITY, UT N305WA Incident minor Improper assembly of the wheel during build up in the operator's maintenance facilities.
Nov 11, 1999 PORTLAND, OR N772AS Incident minor Arcing in the electrical system wiring for undetermined reasons.
Nov 02, 1999 JUNEAU, AK N792AS Incident
The failure of the flight crew to provide a recommended landing traffic advisory, and the failure of flight service station personnel to provide a fli…

The failure of the flight crew to provide a recommended landing traffic advisory, and the failure of flight service station personnel to provide a flight advisory to the arriving airplane concerning men and equipment operating on the runway. Factors in the incident were operations at an airport when the control tower was closed, and the failure of the snow plow driver to verify the eminent arrival of the airplane.

Sep 12, 1999 LOS ANGELES, CA N388UA Incident substantial
The lavatory service driver's failure to follow established company procedures and directives. A factor in the accident was the airline's use of a on…

The lavatory service driver's failure to follow established company procedures and directives. A factor in the accident was the airline's use of a one person pushback procedure.

Aug 26, 1999 DURBAN, SF UNK Incident Investigation pending
Mar 04, 1999 BIARRITZ, FR FGBYA Incident substantial Investigation pending
Dec 15, 1998 ORLANDO, FL N327DL Incident minor
A discharged battery due to a loss of electrolyte, and the latent shorted failures of the No. 1 and 2 generator control unit (GCU) blocking diodes (CR…

A discharged battery due to a loss of electrolyte, and the latent shorted failures of the No. 1 and 2 generator control unit (GCU) blocking diodes (CR910) for undetermined reasons. These failures resulted in an excessive current drawn from both GCUs, during the flight crew's attempt to start the auxiliary power unit, that caused the immediate overload (opening) of the AC power supply input fuses (POR fuses) internal to each GCU, and subsequent loss of the No.1 and 2 generators; complete discharge of the battery, and subsequent total loss of electrical power. Contributing to the incident was the incorrect reading of the cockpit DC voltmeter (read higher than actual reading) allowing the flight crew to depart with an unreliable (discharged) battery.

Dec 08, 1998 NEW YORK, NY GCPX Incident
The Cessna pilot's incorrect visual identification of the Boeing 737's altitude, and decision to take evasive action that was not required, which resu…

The Cessna pilot's incorrect visual identification of the Boeing 737's altitude, and decision to take evasive action that was not required, which resulted in the two airplanes coming within 500 feet horizontally, and 0 feet vertically of one another.

Nov 06, 1998 NEWARK, NJ N12318 Incident minor
A loss of torque on the apex nut of the shimmy damper for undetermined reason(s), which resulted in a failure of the shimmy damper, and the subsequent…

A loss of torque on the apex nut of the shimmy damper for undetermined reason(s), which resulted in a failure of the shimmy damper, and the subsequent failure of the lower torsion link of the right main landing gear.

Sep 17, 1998 GUADALAJARA, MX N20643 Incident Investigation pending
Aug 14, 1998 JUNEAU, AK N799AS Incident substantial The flight crew's inadequate recovery from a bounced landing.
Aug 13, 1998 GATWICK, UK GSBEB Incident Investigation pending
Jul 07, 1998 BIRMINGHAM, AL N701GS Incident minor
The improper electronic control unit software logic that permitted the electronic control unit to lock on a failed hydromechanical resolver, which fai…

The improper electronic control unit software logic that permitted the electronic control unit to lock on a failed hydromechanical resolver, which failed due to damage to a wire that was incurred during the manufacturing process, resulting in an uncommanded and sudden increase in fuel flow to the engine that damaged the turbine and caused the engine to lose power.

Jul 02, 1998 BRAZIL, BR PTTEN Incident Investigation pending
Jun 27, 1998 MUNICH, GE DAHFD Incident Investigation pending
Jun 20, 1998 MARSEILLES, FR FGIXP Incident Investigation pending
May 05, 1998 HAVANA, CU N261LR Incident substantial Investigation pending
Apr 27, 1998 BREMEN, GE DAHLN Incident Investigation pending
Apr 12, 1998 ALMA-ATA, KZ P4NEN Incident substantial Investigation pending
Mar 11, 1998 ANCHORAGE, AK N733AR Incident
The dynamic imbalance in the yaw rate gyro, which provided input to the yaw damper and rudder. A factor was the deteriorated grease in the gyro beari…

The dynamic imbalance in the yaw rate gyro, which provided input to the yaw damper and rudder. A factor was the deteriorated grease in the gyro bearings.

Dec 26, 1997 EUGENE, OR N918UA Incident A checklist procedure was not followed. The initiation of an evacuation was a factor.
Oct 04, 1997 CHICAGO, IL N129SW Incident minor an improper repair to a crack in a brake flange hole on the left main landing gear outboard axle, and subsequent fatigue failure of the axle.
Sep 27, 1997 SEATTLE, WA N13331 Incident
Separation of the ABSB-4 aileron bus cable, resulting in reduced lateral controllability of the aircraft. Related factors were wear in the cable and …

Separation of the ABSB-4 aileron bus cable, resulting in reduced lateral controllability of the aircraft. Related factors were wear in the cable and inadequate inspection of the cable by company maintenance personnel.

Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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