1966 Cessna 150G
Single Engine Piston
Equipment & Features
Aircraft Details
Seller reportedAvionics & Equipment
Description and equipment details provided by the seller. AeroGurus does not verify seller-provided information.
Price Comparison 1 active offer
| Source | Price | Location | Listed | Days on Market | Status | Action |
|---|---|---|---|---|---|---|
|
Seitz Aviation
seitzaviation.com
|
Contact for price
|
— | Apr 05, 2026 | — | Active |
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AeroGurus Data & Analysis
Independent data from FAA, NTSB, and market analysis
About This Cessna 150G
This 1966 Cessna 150G is a 2-seat single engine piston with 1,809 hours on the airframe. There are currently 8 150G aircraft listed for sale with asking prices ranging from $39,950 to $65,000.
Operating costs: Fuel burn is 5.5 GPH (21 L/h), which at current Jet-A prices (~$5.50/gal) means approximately $30/hr in fuel alone. Total variable cost including maintenance reserves is approximately $75/hr. Annual fixed costs (hangar, insurance, crew, annual inspection) average $9,000. With 1,809 hours on the airframe, this aircraft has 591 hours remaining to engine TBO .
NTSB records show 0 incidents for this airframe — a clean safety record. Mechanics have filed 10 service difficulty reports for this type — common maintenance items to discuss during pre-buy.
Pre-Purchase Checklist
Cessna 150G — Model Specs
Model specificationStandard specs for this model. Actual aircraft may differ.
Estimated Cost of Ownership
AeroGurus estimateCESSNA 150G
AeroGurus estimates based on industry averages for the CESSNA 150G. Actual costs vary by location, usage, maintenance history, and configuration. Not a financial quote.
Ownership & Registration
Registration number not available.
Location & Ownership
Aircraft Location
Location not available
Title Status
No FAA title records
Available for US-registered aircraft only
Source: FAA Aircraft Registry, FAA Civil Aviation Registry (DocIndex). Title data may be delayed. Always verify with an aviation attorney before purchase.
Safety Record
NTSB safety data coming soon.
Service Difficulty Reports — Cessna 150G
SDRs are reports filed by mechanics about problems found during maintenance. 10 recent reports for this aircraft type.
LEFT ELEVATOR SEPARATED IN FLIGHT. BOLT CONNECTING ELEVATOR LOOSENED UP AND FELL OUT. ELEVATOR WAS DAMAGED AND APPEARED TO BE BENT FROM AERODYNAMIC FORCES. AIRCRAFT WAS DIFFICULT TO CONTROL. ANY CONTROL MOVEMENT CAUSED UNCONTROLLABLE PITCHING IN TH...
(CAN) VACUUM COUPLING FAILED. PROBLEM FOUND ON START UP AND FLIGHT ABORTED. REPLACED VACUUM PUMP WITH NEW UNIT. ALL WORK PERFORMED BY MAINTENANCE AND SIGNED OUT IN LOGS.
(CAN) CRACK IN THE INTERIOR OF THE RT MUFFLER FOUND DURING ANNUAL ENGINE INSPECTION. NEW MUFFLER TO BE INSTALLED.
(CAN) AIRCRAFT IN CRUISE FLIGHT. PILOT SAW SMOKE AND SHUT DOWN ELECTRICAL POWER TO AIRCRAFT. AIRCRAFT LANDED WITHOUT INCIDENT. INVESTIGATION FOUND RING TERMINAL LAYING ON CABIN HEAT CONTROL. WIRE TRACED BACK AND FOUND CONNECTED TO AMMETER. THIS W...
ROCKER SHAFT BOSSES FOUND CRACKED WHEN CYLINDER REMOVED DUE TO FAILURE. LAST DYE CHECK WAS DONE IN 5/6/2007 (O/H DATE 1998). CYLINDER ONLY HAD 50 HRS SINCE LAST INSPECTION, BUT 5 YEARS CALENDAR TIME. POSSIBLE MORE FREQUENT DYE CHECK ON ROCKER BOS...
TESTED EIGHT REM38S SPARK PLUGS WITH 200 HRS TT AND FOUND THE RESISTORS HAD FAILED, NO RESISTANCE FOUND THROUGH THE SPARK PLUG.
DURING A PRE-PURCHASE INSPECTION, HEAVY CORROSION WAS FOUND AT THE JOINT BETWEEN THE LT STABILIZER SKIN, PN 0432001-55 AND THE RT STABILIZER SKIN, PN 0432001-54 AT THE LOWER CENTER RIVET LINE WHICH HAD EATEN AWAY NUMEROUS RIVETS, LOOSENED THE SKIN JO...
WINGS WERE PREVIOUSLY REMOVED TO FACILITATE TRANSPORTATION. INSPECTION OF THE LT AND RT FWD SPAR BEARING BLOCKS IN THE FUSELAGE (P/N 0411129) FOUND SEVERE CORROSION DAMAGE. IT APPEARS TO BE DISSIMILAR METAL CORROSION BETWEEN THE SPAR BLOCKS AND THE A...
WINGS WERE PREVIOUSLY REMOVED TO FACILITATE TRANSPORTATION. INSP OF THE LT AND RT FWD SPAR BEARING BLOCKS IN THE FUSELAGE (P/N 0411129) FOUND SEVERE CORROSION DAMAGE. IT APPEARS TO BE DISSIMILAR METAL CORROSION BETWEEN THE SPAR BLOCKS AND THE AN3-21A...
ENGINE HAD BAD HESITATION ON TAKEOFF ACCELERATION. SURGING OCCURRED DURING CLIMB WITH RPM FLUCTUATIONS OF +/- 50-75 RPM. AIRCRAFT AND ENGINE FUEL SCREENS WERE REMOVED AND INSPECTED 3 TIMES IN THE LAST 50 HOURS WITH NO EVIDENCE OF CONTAMINATION. FU...
Source: FAA Service Difficulty Reporting System. Shows maintenance issues reported by mechanics for this aircraft type.
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