Mooney M20F Safety Record
Complete NTSB accident and incident history. 167 events recorded from 1982 to 2025.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| May 10, 2002 | Minneapolis, MN | N976SB | Incident | substantial |
The pilot did not attain a proper climb rate during the go-around and the intentional wheels up landing. Factors associated with the accident were th…The pilot did not attain a proper climb rate during the go-around and the intentional wheels up landing. Factors associated with the accident were the inability of the pilot to maintain directional control of the airplane during the landing and the parked airplane that was contacted. |
| Mar 30, 2002 | Grapeland, TX | N9530M | Incident | substantial |
The loss of engine power due to the #2 connecting rod cap separating from the connecting rod. A contributing factor was the limited forward visibilit…The loss of engine power due to the #2 connecting rod cap separating from the connecting rod. A contributing factor was the limited forward visibility due to oil on the windscreen. |
| Aug 29, 2000 | JONESTOWN, PA | N9436V | Fatal (1) | destroyed |
The pilot's delay in aborting the landing, which resulted in a collision with transmission wires. Factors in the accident were the pilot's improper i…The pilot's delay in aborting the landing, which resulted in a collision with transmission wires. Factors in the accident were the pilot's improper inflight decision to attempt a landing with a 14-knot tailwind, and his use of an unapproved pain medication. |
| Jun 03, 2000 | UPLAND, CA | N9207V | Minor | substantial | The failure of the pilot-in-command to maintain directional control of the aircraft on takeoff after the cabin door became ajar. |
| Apr 19, 2000 | TOMBALL, TX | N7038V | Minor | substantial | Engine seizure due to the rupture of an oil cooler line. |
| Jul 31, 1999 | MONTROSE, CO | N9390V | Serious (1) | substantial | The pilot's inadequate preflight planning and preparation and his failure to maintain clearance from the signpost. A factor was the signpost. |
| Jul 19, 1999 | MARSHALL, MN | N7141V | Minor | substantial |
the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landi…the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landing attempt by the pilot. |
| Jun 29, 1999 | LIBERTY, NC | N7114V | Incident | substantial |
Improper inspection of the muffler assembly resulting in erosion going undetected and the rupture of the muffler and shroud while in cruise flight. Th…Improper inspection of the muffler assembly resulting in erosion going undetected and the rupture of the muffler and shroud while in cruise flight. The condition caused melting of portions of the air induction system, loss of engine power, and the pilot's attempted forced landing that resulted in collision with terrain that sheared one main landing gear and fractured the wheel of the other main landing gear. A factor in the accident was the pilot's obscured vision due to smoke in the cockpit. |
| Mar 04, 1999 | CABOOL, MO | N9381M | Fatal (1) | destroyed | The pilot not maintaining an appropriate airspeed during the turn from base to final resulting in a stall. |
| Nov 19, 1998 | UPLAND, CA | N3500X | Serious (1) | destroyed |
Loss of engine power due to water contaminated fuel and the pilot's inadequate preflight inspection of the airplane. A factor was the failure of the …Loss of engine power due to water contaminated fuel and the pilot's inadequate preflight inspection of the airplane. A factor was the failure of the owner/pilot to properly maintain the airplane. |
| Aug 29, 1998 | FORT COLLINS, CO | N377X | Fatal (2) | destroyed |
The pilot's inadvertent stall/mush due to his excessive angle of bank during his traffic pattern turn to base. Factors were the pilot's improper down…The pilot's inadvertent stall/mush due to his excessive angle of bank during his traffic pattern turn to base. Factors were the pilot's improper downwind altitude, the pilot not properly setting his Kollsman Window in his altimeter, and the high density altitude. |
| May 25, 1998 | LAS VEGAS, NV | N6453Q | Incident | substantial |
The pilot's improper remedial action in controlling the aircraft during a go-around in a crosswind which resulted in a collision with a runway light a…The pilot's improper remedial action in controlling the aircraft during a go-around in a crosswind which resulted in a collision with a runway light and separation of the landing gear. |
| May 24, 1998 | MORIARTY, NM | N6476Q | Incident | substantial | the unfavorable wind condition, and failure of the pilot to adequately compensate for the wind condition during the landing flare. |
| May 17, 1998 | TELLURIDE, CO | N6444Q | Incident | substantial |
The pilot exceeded the crosswind capability performance of the aircraft, and his delayed response in initiating a go around. Factors were gusty, cros…The pilot exceeded the crosswind capability performance of the aircraft, and his delayed response in initiating a go around. Factors were gusty, crosswind and tailwind conditions, and high density altitude. |
| Apr 06, 1998 | LODGEPOLE, MT | N9131V | Fatal (1) | destroyed |
The pilot's failure to maintain clearance from the terrain after flying into an area of known adverse weather. Factors include low ceilings, fog, snow…The pilot's failure to maintain clearance from the terrain after flying into an area of known adverse weather. Factors include low ceilings, fog, snow showers, drizzle, and trees along his intended route. |
| Dec 28, 1997 | FERNCLIFF, VA | N9717M | Minor | destroyed |
the improper installation of the engine oil temperature probe which resulted in oil starvation and a total loss of engine power. A factor in the acci…the improper installation of the engine oil temperature probe which resulted in oil starvation and a total loss of engine power. A factor in the accident was the pilot's overflight of available airports in an effort to reach the 'Nearest Airport' displayed on his loran equipment during the subsequent forced landing. |
| Dec 20, 1997 | SAFFORD, AZ | N2965L | Serious (2) | destroyed |
The pilot's poor in-flight judgement and intentional flight into known adverse weather conditions. Related factors were, mountainous terrain, rain an…The pilot's poor in-flight judgement and intentional flight into known adverse weather conditions. Related factors were, mountainous terrain, rain and fog. |
| Nov 27, 1997 | STUTTGART, AR | N2954L | Incident | substantial |
the pilot's failure to activate the runway lights, which led to his selection of a closed/abandoned runway for the landing. Factors relating to the a…the pilot's failure to activate the runway lights, which led to his selection of a closed/abandoned runway for the landing. Factors relating to the accident were: the unlatched cabin door, and the lack of lighting conditions at dusk. |
| Oct 19, 1997 | COLLEGE STATION, TX | N7433V | Serious (2) | substantial |
The pilot's failure to maintain airspeed during a go-around. Factors were :the pilot's premature retraction of the flaps, his lack of total experience…The pilot's failure to maintain airspeed during a go-around. Factors were :the pilot's premature retraction of the flaps, his lack of total experience in the airplane, the dark night illumination, pilot fatigue, and pressure induced by the passengers to complete the night flight. |
| Sep 11, 1997 | CORAL SPRINGS, FL | N6417Q | Fatal (1) | substantial |
The pilot's misjudging the distance vs. altitude resulting in the collision with the water short of the intended touchdown point of the rough field. …The pilot's misjudging the distance vs. altitude resulting in the collision with the water short of the intended touchdown point of the rough field. Contributing to the accident was the total loss of engine power due to failure of the No. 3 cylinder connecting rod bearing for undetermined reasons and fatigue failure of the No. 3 cylinder connecting rod and piston pin end plugs. |
| Aug 11, 1997 | TALLAHASSEE, FL | N3455X | Fatal (2) | destroyed | fatigue failure of the crankshaft for undetermined reasons. Related factors were: darkness, and obstructions (trees) in the emergency landing area. |
| May 20, 1997 | WHEELING, IL | N6950V | Incident | substantial | binding of the number four exhaust valve, which resulted in a partial power loss. A factor was the ravine. |
| Apr 06, 1997 | MARIETTA, OK | N6492Q | Minor | substantial | The pilot's inadequate short field takeoff. A factor was the pilot's lack of recent experience in short field takeoffs from a grass/turf runway. |
| Dec 26, 1996 | DAYTONA BEACH, FL | N737JC | Incident | substantial |
The pilot's inadequate in-flight fuel consumption calculations, and the excessive flow of the fuel injector servo, that combined to result in fuel exh…The pilot's inadequate in-flight fuel consumption calculations, and the excessive flow of the fuel injector servo, that combined to result in fuel exhaustion. |
| Dec 11, 1996 | WELLSVILLE, NY | N3424N | Fatal (2) | destroyed | Descent below the published minimum descent altitude followed by collision with the surrounding terrain. |