Mooney M20F Safety Record

Complete NTSB accident and incident history. 167 events recorded from 1982 to 2025.

167

All Events

77

Incidents

24

Minor

20

Serious

46

Fatal (101 fatalities)

Date Location Reg# Severity Damage Probable Cause
May 10, 2002 Minneapolis, MN N976SB Incident substantial
The pilot did not attain a proper climb rate during the go-around and the intentional wheels up landing. Factors associated with the accident were th…

The pilot did not attain a proper climb rate during the go-around and the intentional wheels up landing. Factors associated with the accident were the inability of the pilot to maintain directional control of the airplane during the landing and the parked airplane that was contacted.

Mar 30, 2002 Grapeland, TX N9530M Incident substantial
The loss of engine power due to the #2 connecting rod cap separating from the connecting rod. A contributing factor was the limited forward visibilit…

The loss of engine power due to the #2 connecting rod cap separating from the connecting rod. A contributing factor was the limited forward visibility due to oil on the windscreen.

Aug 29, 2000 JONESTOWN, PA N9436V Fatal (1) destroyed
The pilot's delay in aborting the landing, which resulted in a collision with transmission wires. Factors in the accident were the pilot's improper i…

The pilot's delay in aborting the landing, which resulted in a collision with transmission wires. Factors in the accident were the pilot's improper inflight decision to attempt a landing with a 14-knot tailwind, and his use of an unapproved pain medication.

Jun 03, 2000 UPLAND, CA N9207V Minor substantial The failure of the pilot-in-command to maintain directional control of the aircraft on takeoff after the cabin door became ajar.
Apr 19, 2000 TOMBALL, TX N7038V Minor substantial Engine seizure due to the rupture of an oil cooler line.
Jul 31, 1999 MONTROSE, CO N9390V Serious (1) substantial The pilot's inadequate preflight planning and preparation and his failure to maintain clearance from the signpost. A factor was the signpost.
Jul 19, 1999 MARSHALL, MN N7141V Minor substantial
the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landi…

the inadvertent stall and the checklist not followed by the pilot. Contributing factors were the baggage door not secured and the precautionary landing attempt by the pilot.

Jun 29, 1999 LIBERTY, NC N7114V Incident substantial
Improper inspection of the muffler assembly resulting in erosion going undetected and the rupture of the muffler and shroud while in cruise flight. Th…

Improper inspection of the muffler assembly resulting in erosion going undetected and the rupture of the muffler and shroud while in cruise flight. The condition caused melting of portions of the air induction system, loss of engine power, and the pilot's attempted forced landing that resulted in collision with terrain that sheared one main landing gear and fractured the wheel of the other main landing gear. A factor in the accident was the pilot's obscured vision due to smoke in the cockpit.

Mar 04, 1999 CABOOL, MO N9381M Fatal (1) destroyed The pilot not maintaining an appropriate airspeed during the turn from base to final resulting in a stall.
Nov 19, 1998 UPLAND, CA N3500X Serious (1) destroyed
Loss of engine power due to water contaminated fuel and the pilot's inadequate preflight inspection of the airplane. A factor was the failure of the …

Loss of engine power due to water contaminated fuel and the pilot's inadequate preflight inspection of the airplane. A factor was the failure of the owner/pilot to properly maintain the airplane.

Aug 29, 1998 FORT COLLINS, CO N377X Fatal (2) destroyed
The pilot's inadvertent stall/mush due to his excessive angle of bank during his traffic pattern turn to base. Factors were the pilot's improper down…

The pilot's inadvertent stall/mush due to his excessive angle of bank during his traffic pattern turn to base. Factors were the pilot's improper downwind altitude, the pilot not properly setting his Kollsman Window in his altimeter, and the high density altitude.

May 25, 1998 LAS VEGAS, NV N6453Q Incident substantial
The pilot's improper remedial action in controlling the aircraft during a go-around in a crosswind which resulted in a collision with a runway light a…

The pilot's improper remedial action in controlling the aircraft during a go-around in a crosswind which resulted in a collision with a runway light and separation of the landing gear.

May 24, 1998 MORIARTY, NM N6476Q Incident substantial the unfavorable wind condition, and failure of the pilot to adequately compensate for the wind condition during the landing flare.
May 17, 1998 TELLURIDE, CO N6444Q Incident substantial
The pilot exceeded the crosswind capability performance of the aircraft, and his delayed response in initiating a go around. Factors were gusty, cros…

The pilot exceeded the crosswind capability performance of the aircraft, and his delayed response in initiating a go around. Factors were gusty, crosswind and tailwind conditions, and high density altitude.

Apr 06, 1998 LODGEPOLE, MT N9131V Fatal (1) destroyed
The pilot's failure to maintain clearance from the terrain after flying into an area of known adverse weather. Factors include low ceilings, fog, snow…

The pilot's failure to maintain clearance from the terrain after flying into an area of known adverse weather. Factors include low ceilings, fog, snow showers, drizzle, and trees along his intended route.

Dec 28, 1997 FERNCLIFF, VA N9717M Minor destroyed
the improper installation of the engine oil temperature probe which resulted in oil starvation and a total loss of engine power. A factor in the acci…

the improper installation of the engine oil temperature probe which resulted in oil starvation and a total loss of engine power. A factor in the accident was the pilot's overflight of available airports in an effort to reach the 'Nearest Airport' displayed on his loran equipment during the subsequent forced landing.

Dec 20, 1997 SAFFORD, AZ N2965L Serious (2) destroyed
The pilot's poor in-flight judgement and intentional flight into known adverse weather conditions. Related factors were, mountainous terrain, rain an…

The pilot's poor in-flight judgement and intentional flight into known adverse weather conditions. Related factors were, mountainous terrain, rain and fog.

Nov 27, 1997 STUTTGART, AR N2954L Incident substantial
the pilot's failure to activate the runway lights, which led to his selection of a closed/abandoned runway for the landing. Factors relating to the a…

the pilot's failure to activate the runway lights, which led to his selection of a closed/abandoned runway for the landing. Factors relating to the accident were: the unlatched cabin door, and the lack of lighting conditions at dusk.

Oct 19, 1997 COLLEGE STATION, TX N7433V Serious (2) substantial
The pilot's failure to maintain airspeed during a go-around. Factors were :the pilot's premature retraction of the flaps, his lack of total experience…

The pilot's failure to maintain airspeed during a go-around. Factors were :the pilot's premature retraction of the flaps, his lack of total experience in the airplane, the dark night illumination, pilot fatigue, and pressure induced by the passengers to complete the night flight.

Sep 11, 1997 CORAL SPRINGS, FL N6417Q Fatal (1) substantial
The pilot's misjudging the distance vs. altitude resulting in the collision with the water short of the intended touchdown point of the rough field. …

The pilot's misjudging the distance vs. altitude resulting in the collision with the water short of the intended touchdown point of the rough field. Contributing to the accident was the total loss of engine power due to failure of the No. 3 cylinder connecting rod bearing for undetermined reasons and fatigue failure of the No. 3 cylinder connecting rod and piston pin end plugs.

Aug 11, 1997 TALLAHASSEE, FL N3455X Fatal (2) destroyed fatigue failure of the crankshaft for undetermined reasons. Related factors were: darkness, and obstructions (trees) in the emergency landing area.
May 20, 1997 WHEELING, IL N6950V Incident substantial binding of the number four exhaust valve, which resulted in a partial power loss. A factor was the ravine.
Apr 06, 1997 MARIETTA, OK N6492Q Minor substantial The pilot's inadequate short field takeoff. A factor was the pilot's lack of recent experience in short field takeoffs from a grass/turf runway.
Dec 26, 1996 DAYTONA BEACH, FL N737JC Incident substantial
The pilot's inadequate in-flight fuel consumption calculations, and the excessive flow of the fuel injector servo, that combined to result in fuel exh…

The pilot's inadequate in-flight fuel consumption calculations, and the excessive flow of the fuel injector servo, that combined to result in fuel exhaustion.

Dec 11, 1996 WELLSVILLE, NY N3424N Fatal (2) destroyed Descent below the published minimum descent altitude followed by collision with the surrounding terrain.
Disclaimer: This data is sourced from the NTSB Aviation Accident Database. NTSB events reflect reported accidents and incidents and do not necessarily indicate a defect in the aircraft type. Many events involve pilot error, weather conditions, maintenance issues, or other factors unrelated to the aircraft design. This information is provided for research purposes only — consult official NTSB reports for complete details.
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