Hughes 369 Safety Record
Complete NTSB accident and incident history. 434 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Jun 23, 2017 | Dennis, WV | N765KV | Incident | substantial |
The unporting of fuel due to the helicopter's nose-up attitude during long line operations, which resulted in fuel starvation and a total loss of engi…The unporting of fuel due to the helicopter's nose-up attitude during long line operations, which resulted in fuel starvation and a total loss of engine power. |
| Sep 09, 2016 | Peach Orchard, MO | N500TN | Incident | substantial |
The helicopter pilot’s failure to maintain sufficient separation between the main rotor blade and a power line during line guard installation, which r…The helicopter pilot’s failure to maintain sufficient separation between the main rotor blade and a power line during line guard installation, which resulted in an electrical arc to the main rotor. |
| Mar 26, 2016 | Jamestown, ND | N721RP | Incident | substantial | The pilot's excessive descent rate while flaring during a practice autorotation with a power recovery, which resulted in an impact with terrain. |
| Nov 24, 2015 | Carlisle, WA | N50713 | Incident | substantial |
A total loss of engine power during cruise flight due to fuel exhaustion. Contributing to the accident was the improper calibration of the fuel quanti…A total loss of engine power during cruise flight due to fuel exhaustion. Contributing to the accident was the improper calibration of the fuel quantity gauge. |
| Oct 30, 2015 | Marion, SC | N920JP | Incident | substantial |
A momentary jam in the tail rotor control system from an undetermined source, resulting in a torsional fracture of the tail rotor control torque tube …A momentary jam in the tail rotor control system from an undetermined source, resulting in a torsional fracture of the tail rotor control torque tube and a loss of helicopter control. |
| Aug 18, 2014 | Saint Peter, MN | N369GN | Incident | substantial | The pilot did not see the wires resulting in the subsequent wire collision. |
| Feb 25, 2014 | Moonlight Creek, New Zealand, NZ | ZK-IQQ | Incident | substantial | <br /><br /> |
| Feb 03, 2014 | Naples, FL | N8618F | Incident | substantial |
The pilot's inadequate flare during the termination of a practice 180-degree autorotation and the flight instructor's delayed remedial action, which r…The pilot's inadequate flare during the termination of a practice 180-degree autorotation and the flight instructor's delayed remedial action, which resulted in the tail rotor contacting the ground. |
| May 15, 2013 | Camdenton, MO | N725M | Incident | substantial | The piece of wood/tree that contacted the main rotor blade during the low altitude tree-trimming flight. |
| Jan 29, 2013 | London, OH | N193M | Incident | substantial |
The pilot's failure to comply with established cold weather operating procedures, which resulted in a total loss of engine power. Contributing to the …The pilot's failure to comply with established cold weather operating procedures, which resulted in a total loss of engine power. Contributing to the accident was the pilot's excessive aft cyclic input during the landing flare, which resulted in main rotor blade contact with the tail boom. |
| Dec 07, 2012 | Pasadena, CA | N818CE | Incident | substantial | An unsecured headset, which struck the leading edge of a tail rotor blade. Contributing to the accident was the pilot's inadequate safety briefing. |
| Mar 11, 2012 | Trading Bay, AK | C-GVEB | Incident | substantial | The pilot's selection of an unsuitable landing site in flat-light conditions, which resulted in an inadvertent dynamic rollover. |
| Dec 21, 2011 | Fall Branch, TN | N500TN | Incident | substantial | The pilot's improper decision to continue a visual flight into instrument meteorological conditions, which resulted in a wire strike. |
| Feb 23, 2011 | Henryetta, OK | N112AS | Incident | substantial | Failure of the cyclic control system for reasons undetermined. |
| Jun 22, 2010 | Paicines, CA | N8305F | Incident | substantial | An in-flight fire for undetermined reasons. |
| Mar 11, 2010 | Naples, FL | N8618F | Incident | substantial |
The pilot's excessive aft cyclic imput during the flare following an practice autorotation, which resulted in main rotor blade contact with the tail b…The pilot's excessive aft cyclic imput during the flare following an practice autorotation, which resulted in main rotor blade contact with the tail boom. |
| Nov 06, 2009 | Baxley, GA | N89ZC | Incident | substantial | A loss of engine power due to fuel starvation resulting from the pilot’s inadequate preflight inspection of the main fuel valve position. |
| Sep 29, 2009 | Palmer, AK | N501SU | Incident | substantial | A partial loss of engine power after take off for an undetermined reason, which resulted in a hard landing. |
| May 30, 2009 | Baltimore, OH | N298SD | Incident | substantial | The pilot's failure to attain a proper touchdown point, and his decision not to perform a go-around. |
| Apr 05, 2009 | Pacific Ocean, PO | N2058X | Incident | substantial | The pilot’s failure to maintain clearance from an object during takeoff from the deck of a fishing vessel. |
| Nov 25, 2008 | Fillmore, UT | N9154F | Incident | substantial |
The loss of engine power due to fuel starvation as a result of a loose fuel filter upper drain cap, which was not properly secured by maintenance pers…The loss of engine power due to fuel starvation as a result of a loose fuel filter upper drain cap, which was not properly secured by maintenance personnel. |
| Aug 18, 2008 | Bonners Ferry, ID | N622PB | Incident | substantial | The pilot's inadequate preflight planning for the takeoff and the helicopter loading that exceeded the lift performance capability of the helicopter. |
| May 14, 2008 | Kekaha, HI | N530R | Incident | substantial | A loss of engine power for undetermined reasons. |
| Jul 22, 2007 | Omak, WA | N69PF | Incident | substantial |
The pilot's failure to maintain clearance from the surface of a pond that he was using as a water bucket refill site, which resulted in a tail rotor s…The pilot's failure to maintain clearance from the surface of a pond that he was using as a water bucket refill site, which resulted in a tail rotor strike to the water's surface and a torsional overload failure of the tail rotor drive shaft. |
| Jul 05, 2007 | Comfrey, MN | N500NC | Incident | substantial | The loss of engine power due to the loose pressure line during aerial application maneuvers which resulted in a hard forced landing. |