Hughes 369 Safety Record
Complete NTSB accident and incident history. 434 events recorded from 1982 to 2026.
| Date | Location | Reg# | Severity | Damage | Probable Cause |
|---|---|---|---|---|---|
| Feb 13, 2026 | Conques sur Orbiel, OF | F-GJLX | Minor | — | Investigation pending |
| Nov 05, 2024 | Waycross, GA | N11AS | Minor | substantial | An encounter with a foreign object, which resulted in a loss of control and collision with terrain. |
| Jan 29, 2024 | Eharting, OF | D-HMIK | Minor | substantial | Investigation pending |
| Jul 09, 2023 | Waldorf, MD | N5027P | Minor | substantial |
Fatigue failure of the overrunning clutch outer race and a subsequent inflight loss of power due to abnormal bending loads as a result of improper rea…Fatigue failure of the overrunning clutch outer race and a subsequent inflight loss of power due to abnormal bending loads as a result of improper reassembly of the clutch subassembly following maintenance and the presence of microcracks on the clutch’s outer race. |
| Feb 19, 2018 | Pacific Ocean, PO | N501VS | Minor | substantial |
An in-flight mechanical malfunction with the helicopter, which necessitated a ditching in the ocean. The reason for the malfunction could be determine…An in-flight mechanical malfunction with the helicopter, which necessitated a ditching in the ocean. The reason for the malfunction could be determined because the helicopter sank and was not recovered. |
| Jul 27, 2016 | Senheim, GE | D-HMIC | Minor | substantial | Investigation pending |
| Aug 04, 2015 | Ramatuelle, France, FR | D-HBRM | Minor | substantial | Investigation pending |
| Sep 12, 2013 | Kalalau, HI | N519PA | Minor | substantial | The entanglement of a tarp in the helicopter's main rotor from a nearby trash bundle. |
| Jul 29, 2013 | Center Point, WV | N31HM | Minor | substantial |
A total loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any a…A total loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation. |
| Jan 10, 2013 | Kammenniemi, FI | OH-HNP | Minor | substantial | Investigation pending |
| Nov 27, 2012 | Sheridan, OR | N163PJ | Minor | substantial |
The pilot’s failure to prevent the helicopter from entering a vortex ring state (settling with power) condition during an external load operation, whi…The pilot’s failure to prevent the helicopter from entering a vortex ring state (settling with power) condition during an external load operation, which resulted in the helicopter’s main rotor blades impacting the truck. |
| Mar 30, 2012 | McCormick, SC | N868W | Minor | substantial | The pilot's decision to use automotive fuel instead of the approved alternate fuel, which resulted in a total loss of engine power. |
| Mar 08, 2011 | Meeker, CO | N131AL | Minor | substantial | Main rotor contact with the tail boom resulting in tail boom separation. |
| Apr 24, 2007 | Whiteville, NC | N11AS | Minor | substantial |
A partial loss of engine power due to fatigue fracture of the power turbine governor spring, causing a false pneumatic signal to the fuel control and …A partial loss of engine power due to fatigue fracture of the power turbine governor spring, causing a false pneumatic signal to the fuel control and a corresponding reduction in fuel flow. |
| Apr 20, 2007 | Kahuku, HI | N911FT | Minor | substantial |
Fatigue cracking of the oil line from the engine gearbox to the oil pressure gauge, which resulted in loss of engine lubricating oil, leading to seizu…Fatigue cracking of the oil line from the engine gearbox to the oil pressure gauge, which resulted in loss of engine lubricating oil, leading to seizure of the power turbine. |
| May 28, 2006 | Mattituck, NY | N9244F | Minor | substantial | A loss of engine power due to undetermined reasons. |
| Oct 04, 2005 | Hangelosa, SW | SE-HVY | Minor | substantial | Investigation pending |
| Jul 19, 2005 | Loveland, CO | N530TJ | Minor | destroyed |
The pilot's failure to maintain aircraft control due to delayed remedial action during the encounter with the loss of tail rotor effectiveness. Contr…The pilot's failure to maintain aircraft control due to delayed remedial action during the encounter with the loss of tail rotor effectiveness. Contributing factors were the pilot's inadequate preflight performance planning, and the inadequate supervision by the US Forest Service personnel. |
| Apr 27, 2005 | Quantico, VA | N5252Y | Minor | substantial |
The flight crew's failure to maintain adequate altitude/clearance from a building, which resulted in contact with the building, dynamic rollover, and …The flight crew's failure to maintain adequate altitude/clearance from a building, which resulted in contact with the building, dynamic rollover, and collision with terrain. |
| Oct 21, 2003 | Evansville, MN | N49TJ | Minor | substantial |
The pilot's misjudgment of clearance from the surface of the lake during the aerial application pass. The low altitude operation, glassy water, and …The pilot's misjudgment of clearance from the surface of the lake during the aerial application pass. The low altitude operation, glassy water, and his visual perception were contributing factors. |
| Jul 21, 2003 | KETCHIKAN, AK | N1091S | Minor | substantial |
The improper installation of a bolt in the gas generator governor linkage by company maintenance personnel, which resulted in a loss of the bolt, a lo…The improper installation of a bolt in the gas generator governor linkage by company maintenance personnel, which resulted in a loss of the bolt, a loss of engine power while maneuvering, and subsequent forced landing and collision with trees. Factors contributing to the accident were an inadequate preflight inspection by the pilot, and an uncommanded surge in engine power. |
| Jun 30, 2003 | Chung Cheong, KS | HL-9140 | Minor | substantial | Investigation pending |
| Apr 07, 2003 | Taholah, WA | N5225C | Minor | substantial |
The entanglement of the fuel quantity sender float in the start pump wiring within the fuel tank as a result of the wiring not being properly secured.…The entanglement of the fuel quantity sender float in the start pump wiring within the fuel tank as a result of the wiring not being properly secured. This rendered the fuel gauge inaccurate and the low fuel warning light inoperative which led to fuel exhaustion. The improper securing of the wiring was a result of unspecified maintenance personnel not identifying the unsecured condition. Contributing factors were the lack of adequate guidance in the maintenance manuals on inspection of the wiring and the low rotor RPM during the autorotation resulting in a hard landing. |
| Sep 17, 2002 | O'Neill, NE | N500EK | Minor | substantial |
A loss of engine power due to turbine blade separation as a result of hot corrosion damage to the turbine blades. Contributing to the accident was th…A loss of engine power due to turbine blade separation as a result of hot corrosion damage to the turbine blades. Contributing to the accident was the pilot misjudging the flare at the completion of the autorotation resulting in a hard landing. The dark night was a factor. |
| Sep 15, 2002 | Burtonsville, MD | N336SP | Minor | substantial | The failure of the tailrotor gearbox for undetermined reasons. |